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ER Audio ESL-3B speaker kit progress, 22 May07.
Some of you may have been following my reported progress with trying to build a pair of ER Audio ESL-IIIB kits which were purchased by a customer of mine from http://www.eraudio.com.au/index.html I have had the job of "assembling" these kits to a satisfactory level of operation. I got started back in about February this year and could not proceed as quickly as planned because of difficulties encountered resulting from the poor design of the kits. Before people think I have no prowess at building kits or speakers or amplifiers, just take a look at my website at http://www.turneraudio.com.au and compare the amount of information and depth of understanding compared with the all too brief techno info at the ER Audio site. At the ER site there is no proper electronic schematic for the ESL3B as it should be, no impedance measurements, and no measured performance data. These should be stated with ESL, because some amps will NOT be able to drive the ER speakers, whereas the speakers at my site are all easily drivable, and everyone knows about SEAS drivers being OK, so nothing I have made is any worse than the best speakers made with SEAS drivers such as Sonus Faber and Vienna Acoustic. I gurantee a flat full range response, ER don't gurantee anything. I have now overcome most of the ERA problems; I was not warned by anything at the ER Audio site. Here is the history so far of what happened, and it includes process details and some solutions worth remembering. The kit was supplied with spacers already glued to the 1,200mm x 550mm frames for the 3 panel speaker. 8 of the 12 machine screws riveted to the 12 stator plates were too long, and I had to cut them down with a Dremel tool to 6mm. Failure to notice if the screws are too long will result in a completely stuffed panel, because the stators frames won't press down flat properly onto the frames they are glued into with polyurethane glue. The only real mistake I made was with the first attempt to stretch a membrane of the 3.5uM gossamer thin mylar membrane. It is just so delicate! It was easy to tear using tape and a spring balance for sequential tensioning. And sure enough it tore, and I had to begin again, and the second attempt went perfectly until I glued the first frame with its stators in place onto the surface of the stretched out membrane using super glue. Unfortunately, a pin hole of invisible size allowed super glue to seep through to the bench underneath, and the membrane was ruined as I lifted the panel off the bench. Its easy to sand it off the frame and clean up to do it again. Could practice make perfect? I was about to learn.... Use of superglue as recommended in the ERA 33 pages of kit instructions was abandoned!!! I sanded down the surface of the MDF sheet I was using as the bench top with very fine 600 grade wet and dry sandpaper to remove whatever might have caused a damn pinhole. The bench sits on top of a heavy oak dining table I built 31 years ago from thick oak planks. ( I don't have dinner parties anymore, and the accoutrements of a gentleman have more productive uses these days ) The third membrane went fine when I stretched it, and I used the polyurethane glue to glue to the frame after painting on the glue thinly to the plastic frame. I learnt that the easiest way to weigh down the frame on top of the membrane already stretched out on the perfectly flat solid bench is with about 24 house bricks. After lowering the frame with wet glue onto the membrane, cover the frame with a damp towel. The moisture in the towel will ensure the polyurethane glue cures well in 24 hours. Place the bricks on top of the towel gently without allowing the frame to slide around. When all bricks are placed, gently go to each prick and press down hard with about 20Kg in turn, and this will help remove air bubbles in the glue. The towel prevents brick particles falling into the speaker panel. You need to be very clean about everything with the construction; I used my loungeroom because of the good lights, and clean environment. Next day I very carefully cut around the edge of the membrane and I had a perfect looking membrane when I lifted the bricks and towel away and lifted the frame. The conductive strip of copper foil was placed on the second frame and there were no problems. This self adhesive strip 4.5m wide by about 0.2mm thick is actually the foil they use around bits of glass used in leadlighting windows, and is easily available. DON'T drill the 4.5mm dia holes for the 12 x 4mm dia plastic bolts too close to spacer edges or else the membrane will not glue to the spacer properly and will begin a tear at the hole. If you don't understand this, you will have torn membranes, and need to relocate bolt holes, after filling up wrong ones, and this is a PITA..... I applied the high resistance coating to the membrane. All seemed to go OK but I used twice more than recomended, and Rob Mackinlay from ER later said I shouldn't use too much. After waiting a week for the coating to cure, I completed the basic assembly with supplied plastic bolts and plastic surrounds and I had a basically completed speaker, but without the timber surround or box for electronics underneath. The kit does not include any surround timber frame or box, and one is left to make all that oneself, its rather like being given a speaker kit with drivers but without a box. I can only imagine the terrible attempts being made by amateur audiophiles who have no carpentry or joinery making skills or tools. You won't want to see their speakers pictured on the Web. Then came time to hook up the input transformer and build the not supplied board for a suitable cross over for the speakers. I designed and built the un-supplied crossover and required board. The electronic parts supplied were a regulated LV dc power supply which can be adjusted for its dc level. This then feeds a supplied EHT supply which converts the sub 10Vdc to up to about -5.5kV for application to the membrane. The EHT supply is connected with -EHT voltage taken to the copper foil strip around the frames and the ground terminal of the EHT supply is taken to the CT of the SUT secondary. The SUT is supplied, but has half the core size and half the primary turns really needed for saturation proof operation. I have advised ER Audio with full details of an alternative design for their transformer, and i look forward to them addopting my recomendations. The supplied SUT has far too thin P to S insulation, resulting in 390pF of shunt capacitance appearing across the secondary, which transforms to massive 3.16uF at the primary. The treble panel has 100pF capacitance which transforms to 0.81uF, and the total input capacitance seen by the amplifier = 4uF, ( about twice what Quad ESL57 managed ). The bass panel capacitance of 800pF transforms to 6.5uF at the primary, but the series resistance prevents this much C ever being experienced as a load on the amp, so bass panel C is quite entirely benign. I tried a very basic crossover network about which I will have more to say, and hooked up the speaker and tranny to an amplifier capable of 21Vrms max into a high Z load, and up to 70 watts into 3 ohms, 14.5Vrms. Output Z was 0.2 ohms, BW 7Hz to 30kHz, 2 ohms connected at low levels, and THD 0.2% at max po into 8 ohms, 50 watts, 18Vrms, and mainly class A with a quad of mosfets. I turned on the EHT and gradually increased the EHT until I heard all kinds of spluttery spittery sounds and saw numerous blue discharges occuring all over the panels. I backed off immediately until the noises stopped and conducted sound tests using pink noise and test gear as described in my speaker building pages at http://www.turneraudio.com.au/loudspeakers-diy.html Then I began testing the responses at 1M, 2M ,4M distances at a 1.2M off floor level, on axis, with the speaker taped temporarily to a stout dining chair I also built 31 years ago. Bottom of the speaker is 450mm above the floor, speaker is vertical. I got a truly appalling response. The sensitivity seemed appallingly low. For the same quite low level of pink noise, I needed maybe 5 times the voltage I'd need for my own Sublimes shown at http://www.turneraudio.com.au/loudspeakers-new.html The power handling was atrocious, and LF capablity suffered from arcing and distortions. My customer visted me in the middle of testing and was not impressed at all. We talked about quitting, but I ain't no bloody quitter. I obtained the loan of a high impedance HV probe to measure up to 20kV safely, and found that any EHT increase above 2.2kV cause horrid discharge noise and premature clipping. ESL sensitivity is about proportional to applied EHT voltage, and I wanted to be able to apply 5,000V if possible, like ESL57 and ESL63. I then thought that the arcing seen must be because the poor insulation qualities of the black powder coating on the suplied stators. So I stripped off membrane No 3, and coated all the stators with two generous coats of anti corona paint, Isonel 642, and put on a new membrane No 4 but with two very thin conductive coats on the membrane, this time using the right total amount and to get an even coating. I also placed in the pattern of 10 anti resonance silicone pads but that made no difference to following results. I re-tested after the rebuild and curing times, and although there was not such a lot of arcing and EHT leakage, the response and problems were quite unacceptable. I turned off the EHT supply, and considered using more membrane tension of 2Kg / 60mm of side length, not the low 0.8Kg recommended. ESL63 use 2.5Kg for the same material. Lots of crackling noises continued for minutes after turn off of the EHT and after the voltage had rapidly fallen to 0V. It was the membrane partially releasing from its stuck position. When I unbolted the two halves of the speaker the next day after the dismal tests, I found that about 70% of the area of both bass membranes had become glued to the stators on the side away from that where the membrane is coated. I was able to gently prise the membrane off the starors with a bit of bent copper wire poked through slots in the stators. Anti corona paint is slightly sticky with mylar. No wonder I had such horrible test results. But it had taken two attempts before I became aware of the problem and I guess that EVERY SILLY MAN WHO TRIES TO USE ABOVE ABOUT 3KV will have what I call membrane "stiction" problems. There are posts I've seen in these silly little private forums where they all bull**** to each other of guys cranking up the EHT and I believe they don't realize their problems. With stuck membranes, the speakers still work at mid & treble, but poorly, and definitely not as intended, and with queer bass. Back to my drawing board I went, and at this point I didn't think it would be wise to consult ER Audio for advice, and I posted on these groups to see if anyone else had had problems. One Collin Topps of the UK answered my initial posts to groups in private emails which began cordially, but ended rudely. Collin is the UK ERA sales rep. He said repeatedly nobody has had any problems building ER Audio panels. He refused to accept that I was having serious bothers, or offer any advice that was relevant and useful. Then he ended up telling me to sod off, and I thought that this technically dumb salesman in the UK acting for ER Audio as their sales agent has some basic things about public relations he has yet to learn. He'd sure never get a job selling anything I made. I continued to post on the panels and learn more about ESL construction from other ESL amateur productions around the world. Since then, I decided that the membrane must not be allowed to travel too close to a stator, ideally not more than half the actual distance between membrane and stator surface, so if this is 4mm, as it is in ESL57 bass panels, then 2mm is enough maximum movement distance. Quad achive this by using 2mm thick PVC plastic sheeting for bass stators, with conductive stator material being conductiove paint on the outside of the perforated plastic sheeting. So the membrane CANNOT move more than 2mm and cannot be less than 2mm away from the stator surface. The of force of electrostatic attraction increases proportionally to 1/d squared, so if d is only a few thousanths of an inch, F becomes huge. No wonder my ERA membranes were sticking like cling wrap around a pumpkin at the grocer. The bass panel membrane to stator distance in ERA panels is 2.4mm. I thought that if I applied about 0.8mm of non conductive material to the inside surface of the stator, It would keep the membrane getting too close to a stator, and the extra tension would always overcome the force caused by the EHT without signal. I'd have 1.6mm for membrane movement, not as much as in a Quad speaker, but enough. So I applied four coats of silicone paint made from roof and gutter silicone sealant bought for $5 per tube at a plumber's store. To coat all the stators for one speaker I used 1.3 tubes of silicone, and about 600ml of white spirit for thinning. The thinning is done by using a small cheap brush with dabbing action in a clean tuna fish can until the paint has thick honey consistency and no visible lumps. The silicone is applied by dabbing action with the brush laid flat on the perforated steel sheeting, not letting silicone close off perforation holes. It self levels fairly well, and partially wraps around the sharp metal edges of the holes in the stators, so probably enhances air flow caused by sound waves. 24 hours is fine between coats of silicone. It sticks well to the anti corona paint I already have on the stators. The silicone becomes rubbery, and smooth surfaced, even though some uneveness of this coating thickness occurs, but basically, I got the right amount of goop applied to all stator surfaces. I finally stretched membrane No 5 last week and have re-assembled the speaker for a new test. After the frame was first glued to the stretched and much tighter membrane, I still found the membrane tended to stick to the stator if pressed over to it gently by hand. So I then bought a small can of Johnson's Baby Powder and squirted in a lot of powder through perforations, and with an air blower, blew it all around everywhere. Then i sucked off the excess woth a gentle vacuum cleaner. On the opposite second frame and stators, i just dusted the powder on and removed excess with vacuum. The panel was then re-assembled. Did my ingenuity prevent the problems I was having? After connection of the speaker to the amp and without signal, I raised the EHT and at 3.2kV while I watched the bass membranes carefully I saw them whip over to a stator and remain hard against it. Hmm, same old problem. However, when i reduced EHT, the membrane let go without all the crackling sounds they'd made previously after turn off of the EHT supply. The powdered layer of rubber was doing the right kind of trick in preventing stiction. I was able to leave the EHT on all night at 3kV, but just occasionally, some small click noise would occur, so i have settled on having 2.7kV as the maximum EHT voltage which could be safely applied to these panels before problems would occur. I began to seriously test the speaker response and do serious comparisons again with my own blameless Sublimes. They sit side by side, and comparisons can be fairly made, same room, 200Cubic metres, well out from a wall, well damped etc. The same amps, test signal, test gear and mic is used to eliminate any chance of making an unfair comparison. Finally, I got the speakers to measure +/- 2dB between LF pole = 35Hz and HF pole = 22kHz, and to give as flat a response as I could get without adding a ridiculous number of crossover compensation networks. This response was measured at 3M with mic 800mm above the floor, and about exactly how they will be listened to in my customer's room, which is not quite as good as my own, but measurement of his existing speaker response has been little different to what i get in my rooms. If I get speakers to sound well here, they always travel well. My impressions with the sound with music is good, but the 50 watt class A amps I have been using for trials run completely out of headroom at only modest levels equal to about 1/3 watt average into my Sublimes which are 5.6 ohms average, and have 88dB/W/M watt sensitivity. After numerous calculations, I figured I needed 5 times the applied voltage for the same SPL with ERA panels compared to my own speakers. At least a 100 watt amp would be needed for quite modest levels of sound, not because 100 watts would ever be generated, but merely to get enough voltage. Collin Tops said he was using an SET amp with 16 watts only, and maybe he likes quietspeakers. But I prefer loudspeakers. And for these ERA quietspeakers, there is not the slightest bit of speaker protection circuitry included as it is in Quad ESL63. What is the safe maximum voltage? not as much as for Quads, that's for sure. Anyway, I did clip the 50 watt amp a few times when i tried to go loud with some busy Salsa music from Buena Vista Social Club, and nothing bad happened, so the 6 coats of goop I have on the stators seemes to resist arcing. A 16 watt SET amp with Rout 2ohms would be a horrible thing to drive such ESL. There would be a serious HF roll off, but perhaps Collin is an old giza with stuffed hearing, and so may not mind if the HF pole = 6kHz. And without my networks and crossovers, the response could be worse, peaked up high between 500 and 6kHz, ie, without bass or treble. He will have to conduct all the same well conducted tests i have done before he'd ever know WTF he's actually built. He should not be offended when I say I don't trust what salesmen tell me. Nobody from ERA has had the courage to discuss their speakers in the public forums. I have just measured the Z, and with the details of networks below got the following Z figures:- 10Hz, approx 80ohms, 20Hz, 41, 50Hz, 14, 60Hz, 11, 80Hz, 10, 110Hz, 11, 200Hz, 18, 300Hz, 20, 500Hz, 19, 1kHz, 15, 2kHz, 11.5, 10kHz, 5, 20kHz, 3, 40kHz, 2. If you plot the above points on a graphed sheet of log paper, and join the dots with gentle curves and you will have the Z. The average Z between 50Hz and 2kHz = 14 ohms. Therefore a tube amp set up for a match to 16 ohms will work, but it'd need to be able to make 30Vrms, which is 64 watts into 14 ohms. The amount of signal above 2kHz which feeds the low Z average of 5ohms between 2khz and 20kHz is small, and as long as the Rout 0.5 ohms there will not be a serious loss of HF detail. One of my 8585 tube amplifiers with a quad of KT90 in PP per channel is powering 3 stacked pairs of ESL57 no problems, even though the Z = 0.6 ohms at 18kHz. But 16 watts from SET would be hopless, unless you had the speakers so close they are like giant ESL headphones. DO NOT use the recommended circuit resistances so vaguely shown in the ER instructions. I found that the best way to hook up the ESL-3B speakers is as follows:- BEFORE the the input to the primary of the step up transformer, ( SUT ):- Make a series L + R network of 4mH plus 27 ohms. Connect this across the P winding. Connect one end of the P winding to the 0V terminal for the black lead from the amplifier. To the other live primary end, connect a series C & R network of 150uF plus 1.5ohms across to the speaker terminal to which the red wire from the amp connects. These two input networks will have several effects. The 27 ohms plus 4mH makes the input loaded with 27 ohms at low F, thus damping the low Z of the series 150uF and primary shunt inductance of 32 mH. The 150uF will prevent LF entering the speaker and causing the rather poor quality SUT from saturating all too easily with high transient LF voltages. The -3dB cut off is at 50Hz, and the attenuation is second order, barely enough. To get better headroom for these speakers, use a second input cap in series of 100uF, giving -3db at about 100Hz, then use a sub. More signal will be then applicable above 100Hz. The 1.5 ohms adds to the 0.5 ohms of SUT winding resistance which is important to damp the series resonance between the awfully high amount of shunt capacitance in the SUT and the leakage inductance at around 20kHz. Therefore input resistance is a minimum of 2ohms by 50kHz, so not many amps should blow up. AFTER the secondary of the SUT, place the following networks from each end of sec to the bass panel terminals:- You will need the following parts, 16 x 100k resistors, metal film, 1%, 2 watt rated. 2 x 0.0033uF capacitors rated at 4kV. Find good quality polypropylene caps. To each bass stator, connect 100k to a pair of common points for the rear and front pairs of bass panels, Then series 4 x 100k to make 400k from each common point to the ends of the SUT secondary. To each treble stator, connect a parallel pair of 100k to make 50k to a pair of common points for front and rear stators. From the common points, connect the 0.0033uF to the sec ends of the SUT. The 0.0033uF plus 50k form a CR HPF. MAKE SURE the treble panel with its crossover is REVERSE PHASE CONNECTED TO THE BASS PANELS. The -3dB points in the signals in the electronic circuit thus created is 160Hz for bass, with signal rolling off at 6dB/octave above 160Hz, and 700Hz for the treble panels, also rolling off at 6dB/octave. Keeping pass signals out of the treble panel is a good idea. The speaker phase shift will be maximally quite large, but maybe under 60degrees, but I found the treble acoustic signal produced by the bass panels will affect the treble panel badly if not phase reversed ( like many other dynamic speakers ), and despite the attenuation by the R & C filter LPF effect of bass series R and the bass panel capacitance which totals 800pF. The ONLY way I could flatten the response and remove what was a wide 6dB dip in the resonse at 5kHz with reverse phase connections. This what I measured, and the acoustic response has little corelation to the signal applied. I will perhaps draw all the relevant curves of bass and treble signals applied and and include all this info at a website page. I hope to include a schematic of the equivalant LCR model of the the panels and SUT. I hope there would be a net positive result amoung builders of ESL. This should all have a very positive effect on understanding of what is really involved to make a pair of ESL speakers. Hopefully, all of what i say will fertilize the minds who created the ER Audio ESL speakers. They can scream long and hard at my critique, and i don't give a ****, their marketing is quite deceptive, and they say it'll be easy, and take only so long, but no, its not true, and they are bull****ting, and the total time I will end up spending on R&D, and patching up the mess of the thing they supplied plus do all the woodwork will amount to 10 times the time they say. My customer here was lulled into the project, along with me, under what now seem like false statements about the product. Had I known of all the difficulties and parts quality and non inclusions, i would never ever have agreed to my building of one of these kits after my customer bought it. He isn't technically minded, and could NEVER EVER have successfully built a kit from ERA. If I allowed quite low trade rates of $50 per hour to build these speakers and fix problems and do R&D, I would find I would be entitled to claim a payment of maybe $5,000 for the labour of building these speakers, plus the cost of supply of items not included, about $400. being a gentleman I won't ask more than a fraction of the figure from my customer, but frankly, the sooner I see these speakers leaving my workshop, the better, and I don't ever want to build another pair that I did not fully design myself!!!!! The original kit price was $2,000, and so the whole deal of up $7,400 value is quite poor value when a fully restored/rebuilt pair of Quad ESL57 could be had for about $4,000 from one John Hall in Melbourne. I have a Quad ESL57 which is unrestored and it even outperforms the ERA on most counts. How anyone could say the ERA speaker is better product than a Quad ESL57 or ESL63, as some have suggested is quite beyond me; maybe these people had old speakers with lots of faults, and replaced them with ERA because they thought they'd be better. The other complaint I have about the ESL3B is that its ONE panel, not two bass with one treble, like ESL2B. This means that if a membrane tears or ****s up in just one of the 3 sub panels, the WHOLE 3 subpanels have to be fixed, rather than just fix one of the 3 sub panels. There is BS spiel about why the ESL3B is a better than others, but ERA are pushing the flat ESL3B because it appears to me the cost of production is less for the less complex product. but the repair bills for YOU, the buyer, will always be higher. All the comparisons one reads make silly one liner statements without the pages of detailed back ups. So don't make me waste more time reading your replies which are not backed up with facts. Patrick Turner. |
ER Audio ESL-3B speaker kit progress, 22 May07.
"Patrick Turner" wrote in message ... Some of you may have been following my reported progress with trying to build a pair of ER Audio ESL-IIIB kits which were purchased by a customer of mine from http://www.eraudio.com.au/index.html I have had the job of "assembling" these kits to a satisfactory level of operation. I got started back in about February this year and could not proceed as quickly as planned because of difficulties encountered resulting from the poor design of the kits. Before people think I have no prowess at building kits or speakers or amplifiers, just take a look at my website at http://www.turneraudio.com.au and compare the amount of information and depth of understanding compared with the all too brief techno info at the ER Audio site. At the ER site there is no proper electronic schematic for the ESL3B as it should be, no impedance measurements, and no measured performance data. These should be stated with ESL, because some amps will NOT be able to drive the ER speakers, whereas the speakers at my site are all easily drivable, and everyone knows about SEAS drivers being OK, so nothing I have made is any worse than the best speakers made with SEAS drivers such as Sonus Faber and Vienna Acoustic. I gurantee a flat full range response, ER don't gurantee anything. I have now overcome most of the ERA problems; I was not warned by anything at the ER Audio site. Here is the history so far of what happened, and it includes process details and some solutions worth remembering. The kit was supplied with spacers already glued to the 1,200mm x 550mm frames for the 3 panel speaker. 8 of the 12 machine screws riveted to the 12 stator plates were too long, and I had to cut them down with a Dremel tool to 6mm. Failure to notice if the screws are too long will result in a completely stuffed panel, because the stators frames won't press down flat properly onto the frames they are glued into with polyurethane glue. The only real mistake I made was with the first attempt to stretch a membrane of the 3.5uM gossamer thin mylar membrane. It is just so delicate! It was easy to tear using tape and a spring balance for sequential tensioning. And sure enough it tore, and I had to begin again, and the second attempt went perfectly until I glued the first frame with its stators in place onto the surface of the stretched out membrane using super glue. Unfortunately, a pin hole of invisible size allowed super glue to seep through to the bench underneath, and the membrane was ruined as I lifted the panel off the bench. Its easy to sand it off the frame and clean up to do it again. Could practice make perfect? I was about to learn.... Use of superglue as recommended in the ERA 33 pages of kit instructions was abandoned!!! I sanded down the surface of the MDF sheet I was using as the bench top with very fine 600 grade wet and dry sandpaper to remove whatever might have caused a damn pinhole. The bench sits on top of a heavy oak dining table I built 31 years ago from thick oak planks. ( I don't have dinner parties anymore, and the accoutrements of a gentleman have more productive uses these days ) The third membrane went fine when I stretched it, and I used the polyurethane glue to glue to the frame after painting on the glue thinly to the plastic frame. I learnt that the easiest way to weigh down the frame on top of the membrane already stretched out on the perfectly flat solid bench is with about 24 house bricks. After lowering the frame with wet glue onto the membrane, cover the frame with a damp towel. The moisture in the towel will ensure the polyurethane glue cures well in 24 hours. Place the bricks on top of the towel gently without allowing the frame to slide around. When all bricks are placed, gently go to each prick and press down hard with about 20Kg in turn, and this will help remove air bubbles in the glue. The towel prevents brick particles falling into the speaker panel. You need to be very clean about everything with the construction; I used my loungeroom because of the good lights, and clean environment. Next day I very carefully cut around the edge of the membrane and I had a perfect looking membrane when I lifted the bricks and towel away and lifted the frame. The conductive strip of copper foil was placed on the second frame and there were no problems. This self adhesive strip 4.5m wide by about 0.2mm thick is actually the foil they use around bits of glass used in leadlighting windows, and is easily available. DON'T drill the 4.5mm dia holes for the 12 x 4mm dia plastic bolts too close to spacer edges or else the membrane will not glue to the spacer properly and will begin a tear at the hole. If you don't understand this, you will have torn membranes, and need to relocate bolt holes, after filling up wrong ones, and this is a PITA..... I applied the high resistance coating to the membrane. All seemed to go OK but I used twice more than recomended, and Rob Mackinlay from ER later said I shouldn't use too much. After waiting a week for the coating to cure, I completed the basic assembly with supplied plastic bolts and plastic surrounds and I had a basically completed speaker, but without the timber surround or box for electronics underneath. The kit does not include any surround timber frame or box, and one is left to make all that oneself, its rather like being given a speaker kit with drivers but without a box. I can only imagine the terrible attempts being made by amateur audiophiles who have no carpentry or joinery making skills or tools. You won't want to see their speakers pictured on the Web. Then came time to hook up the input transformer and build the not supplied board for a suitable cross over for the speakers. I designed and built the un-supplied crossover and required board. The electronic parts supplied were a regulated LV dc power supply which can be adjusted for its dc level. This then feeds a supplied EHT supply which converts the sub 10Vdc to up to about -5.5kV for application to the membrane. The EHT supply is connected with -EHT voltage taken to the copper foil strip around the frames and the ground terminal of the EHT supply is taken to the CT of the SUT secondary. The SUT is supplied, but has half the core size and half the primary turns really needed for saturation proof operation. I have advised ER Audio with full details of an alternative design for their transformer, and i look forward to them addopting my recomendations. The supplied SUT has far too thin P to S insulation, resulting in 390pF of shunt capacitance appearing across the secondary, which transforms to massive 3.16uF at the primary. The treble panel has 100pF capacitance which transforms to 0.81uF, and the total input capacitance seen by the amplifier = 4uF, ( about twice what Quad ESL57 managed ). The bass panel capacitance of 800pF transforms to 6.5uF at the primary, but the series resistance prevents this much C ever being experienced as a load on the amp, so bass panel C is quite entirely benign. I tried a very basic crossover network about which I will have more to say, and hooked up the speaker and tranny to an amplifier capable of 21Vrms max into a high Z load, and up to 70 watts into 3 ohms, 14.5Vrms. Output Z was 0.2 ohms, BW 7Hz to 30kHz, 2 ohms connected at low levels, and THD 0.2% at max po into 8 ohms, 50 watts, 18Vrms, and mainly class A with a quad of mosfets. I turned on the EHT and gradually increased the EHT until I heard all kinds of spluttery spittery sounds and saw numerous blue discharges occuring all over the panels. I backed off immediately until the noises stopped and conducted sound tests using pink noise and test gear as described in my speaker building pages at http://www.turneraudio.com.au/loudspeakers-diy.html Then I began testing the responses at 1M, 2M ,4M distances at a 1.2M off floor level, on axis, with the speaker taped temporarily to a stout dining chair I also built 31 years ago. Bottom of the speaker is 450mm above the floor, speaker is vertical. I got a truly appalling response. The sensitivity seemed appallingly low. For the same quite low level of pink noise, I needed maybe 5 times the voltage I'd need for my own Sublimes shown at http://www.turneraudio.com.au/loudspeakers-new.html The power handling was atrocious, and LF capablity suffered from arcing and distortions. My customer visted me in the middle of testing and was not impressed at all. We talked about quitting, but I ain't no bloody quitter. I obtained the loan of a high impedance HV probe to measure up to 20kV safely, and found that any EHT increase above 2.2kV cause horrid discharge noise and premature clipping. ESL sensitivity is about proportional to applied EHT voltage, and I wanted to be able to apply 5,000V if possible, like ESL57 and ESL63. I then thought that the arcing seen must be because the poor insulation qualities of the black powder coating on the suplied stators. So I stripped off membrane No 3, and coated all the stators with two generous coats of anti corona paint, Isonel 642, and put on a new membrane No 4 but with two very thin conductive coats on the membrane, this time using the right total amount and to get an even coating. I also placed in the pattern of 10 anti resonance silicone pads but that made no difference to following results. I re-tested after the rebuild and curing times, and although there was not such a lot of arcing and EHT leakage, the response and problems were quite unacceptable. I turned off the EHT supply, and considered using more membrane tension of 2Kg / 60mm of side length, not the low 0.8Kg recommended. ESL63 use 2.5Kg for the same material. Lots of crackling noises continued for minutes after turn off of the EHT and after the voltage had rapidly fallen to 0V. It was the membrane partially releasing from its stuck position. When I unbolted the two halves of the speaker the next day after the dismal tests, I found that about 70% of the area of both bass membranes had become glued to the stators on the side away from that where the membrane is coated. I was able to gently prise the membrane off the starors with a bit of bent copper wire poked through slots in the stators. Anti corona paint is slightly sticky with mylar. No wonder I had such horrible test results. But it had taken two attempts before I became aware of the problem and I guess that EVERY SILLY MAN WHO TRIES TO USE ABOVE ABOUT 3KV will have what I call membrane "stiction" problems. There are posts I've seen in these silly little private forums where they all bull**** to each other of guys cranking up the EHT and I believe they don't realize their problems. With stuck membranes, the speakers still work at mid & treble, but poorly, and definitely not as intended, and with queer bass. Back to my drawing board I went, and at this point I didn't think it would be wise to consult ER Audio for advice, and I posted on these groups to see if anyone else had had problems. One Collin Topps of the UK answered my initial posts to groups in private emails which began cordially, but ended rudely. Collin is the UK ERA sales rep. He said repeatedly nobody has had any problems building ER Audio panels. He refused to accept that I was having serious bothers, or offer any advice that was relevant and useful. Then he ended up telling me to sod off, and I thought that this technically dumb salesman in the UK acting for ER Audio as their sales agent has some basic things about public relations he has yet to learn. He'd sure never get a job selling anything I made. I continued to post on the panels and learn more about ESL construction from other ESL amateur productions around the world. Since then, I decided that the membrane must not be allowed to travel too close to a stator, ideally not more than half the actual distance between membrane and stator surface, so if this is 4mm, as it is in ESL57 bass panels, then 2mm is enough maximum movement distance. Quad achive this by using 2mm thick PVC plastic sheeting for bass stators, with conductive stator material being conductiove paint on the outside of the perforated plastic sheeting. So the membrane CANNOT move more than 2mm and cannot be less than 2mm away from the stator surface. The of force of electrostatic attraction increases proportionally to 1/d squared, so if d is only a few thousanths of an inch, F becomes huge. No wonder my ERA membranes were sticking like cling wrap around a pumpkin at the grocer. The bass panel membrane to stator distance in ERA panels is 2.4mm. I thought that if I applied about 0.8mm of non conductive material to the inside surface of the stator, It would keep the membrane getting too close to a stator, and the extra tension would always overcome the force caused by the EHT without signal. I'd have 1.6mm for membrane movement, not as much as in a Quad speaker, but enough. So I applied four coats of silicone paint made from roof and gutter silicone sealant bought for $5 per tube at a plumber's store. To coat all the stators for one speaker I used 1.3 tubes of silicone, and about 600ml of white spirit for thinning. The thinning is done by using a small cheap brush with dabbing action in a clean tuna fish can until the paint has thick honey consistency and no visible lumps. The silicone is applied by dabbing action with the brush laid flat on the perforated steel sheeting, not letting silicone close off perforation holes. It self levels fairly well, and partially wraps around the sharp metal edges of the holes in the stators, so probably enhances air flow caused by sound waves. 24 hours is fine between coats of silicone. It sticks well to the anti corona paint I already have on the stators. The silicone becomes rubbery, and smooth surfaced, even though some uneveness of this coating thickness occurs, but basically, I got the right amount of goop applied to all stator surfaces. I finally stretched membrane No 5 last week and have re-assembled the speaker for a new test. After the frame was first glued to the stretched and much tighter membrane, I still found the membrane tended to stick to the stator if pressed over to it gently by hand. So I then bought a small can of Johnson's Baby Powder and squirted in a lot of powder through perforations, and with an air blower, blew it all around everywhere. Then i sucked off the excess woth a gentle vacuum cleaner. On the opposite second frame and stators, i just dusted the powder on and removed excess with vacuum. The panel was then re-assembled. Did my ingenuity prevent the problems I was having? After connection of the speaker to the amp and without signal, I raised the EHT and at 3.2kV while I watched the bass membranes carefully I saw them whip over to a stator and remain hard against it. Hmm, same old problem. However, when i reduced EHT, the membrane let go without all the crackling sounds they'd made previously after turn off of the EHT supply. The powdered layer of rubber was doing the right kind of trick in preventing stiction. I was able to leave the EHT on all night at 3kV, but just occasionally, some small click noise would occur, so i have settled on having 2.7kV as the maximum EHT voltage which could be safely applied to these panels before problems would occur. I began to seriously test the speaker response and do serious comparisons again with my own blameless Sublimes. They sit side by side, and comparisons can be fairly made, same room, 200Cubic metres, well out from a wall, well damped etc. The same amps, test signal, test gear and mic is used to eliminate any chance of making an unfair comparison. Finally, I got the speakers to measure +/- 2dB between LF pole = 35Hz and HF pole = 22kHz, and to give as flat a response as I could get without adding a ridiculous number of crossover compensation networks. This response was measured at 3M with mic 800mm above the floor, and about exactly how they will be listened to in my customer's room, which is not quite as good as my own, but measurement of his existing speaker response has been little different to what i get in my rooms. If I get speakers to sound well here, they always travel well. My impressions with the sound with music is good, but the 50 watt class A amps I have been using for trials run completely out of headroom at only modest levels equal to about 1/3 watt average into my Sublimes which are 5.6 ohms average, and have 88dB/W/M watt sensitivity. After numerous calculations, I figured I needed 5 times the applied voltage for the same SPL with ERA panels compared to my own speakers. At least a 100 watt amp would be needed for quite modest levels of sound, not because 100 watts would ever be generated, but merely to get enough voltage. Collin Tops said he was using an SET amp with 16 watts only, and maybe he likes quietspeakers. But I prefer loudspeakers. And for these ERA quietspeakers, there is not the slightest bit of speaker protection circuitry included as it is in Quad ESL63. What is the safe maximum voltage? not as much as for Quads, that's for sure. Anyway, I did clip the 50 watt amp a few times when i tried to go loud with some busy Salsa music from Buena Vista Social Club, and nothing bad happened, so the 6 coats of goop I have on the stators seemes to resist arcing. A 16 watt SET amp with Rout 2ohms would be a horrible thing to drive such ESL. There would be a serious HF roll off, but perhaps Collin is an old giza with stuffed hearing, and so may not mind if the HF pole = 6kHz. And without my networks and crossovers, the response could be worse, peaked up high between 500 and 6kHz, ie, without bass or treble. He will have to conduct all the same well conducted tests i have done before he'd ever know WTF he's actually built. He should not be offended when I say I don't trust what salesmen tell me. Nobody from ERA has had the courage to discuss their speakers in the public forums. I have just measured the Z, and with the details of networks below got the following Z figures:- 10Hz, approx 80ohms, 20Hz, 41, 50Hz, 14, 60Hz, 11, 80Hz, 10, 110Hz, 11, 200Hz, 18, 300Hz, 20, 500Hz, 19, 1kHz, 15, 2kHz, 11.5, 10kHz, 5, 20kHz, 3, 40kHz, 2. If you plot the above points on a graphed sheet of log paper, and join the dots with gentle curves and you will have the Z. The average Z between 50Hz and 2kHz = 14 ohms. Therefore a tube amp set up for a match to 16 ohms will work, but it'd need to be able to make 30Vrms, which is 64 watts into 14 ohms. The amount of signal above 2kHz which feeds the low Z average of 5ohms between 2khz and 20kHz is small, and as long as the Rout 0.5 ohms there will not be a serious loss of HF detail. One of my 8585 tube amplifiers with a quad of KT90 in PP per channel is powering 3 stacked pairs of ESL57 no problems, even though the Z = 0.6 ohms at 18kHz. But 16 watts from SET would be hopless, unless you had the speakers so close they are like giant ESL headphones. DO NOT use the recommended circuit resistances so vaguely shown in the ER instructions. I found that the best way to hook up the ESL-3B speakers is as follows:- BEFORE the the input to the primary of the step up transformer, ( SUT ):- Make a series L + R network of 4mH plus 27 ohms. Connect this across the P winding. Connect one end of the P winding to the 0V terminal for the black lead from the amplifier. To the other live primary end, connect a series C & R network of 150uF plus 1.5ohms across to the speaker terminal to which the red wire from the amp connects. These two input networks will have several effects. The 27 ohms plus 4mH makes the input loaded with 27 ohms at low F, thus damping the low Z of the series 150uF and primary shunt inductance of 32 mH. The 150uF will prevent LF entering the speaker and causing the rather poor quality SUT from saturating all too easily with high transient LF voltages. The -3dB cut off is at 50Hz, and the attenuation is second order, barely enough. To get better headroom for these speakers, use a second input cap in series of 100uF, giving -3db at about 100Hz, then use a sub. More signal will be then applicable above 100Hz. The 1.5 ohms adds to the 0.5 ohms of SUT winding resistance which is important to damp the series resonance between the awfully high amount of shunt capacitance in the SUT and the leakage inductance at around 20kHz. Therefore input resistance is a minimum of 2ohms by 50kHz, so not many amps should blow up. AFTER the secondary of the SUT, place the following networks from each end of sec to the bass panel terminals:- You will need the following parts, 16 x 100k resistors, metal film, 1%, 2 watt rated. 2 x 0.0033uF capacitors rated at 4kV. Find good quality polypropylene caps. To each bass stator, connect 100k to a pair of common points for the rear and front pairs of bass panels, Then series 4 x 100k to make 400k from each common point to the ends of the SUT secondary. To each treble stator, connect a parallel pair of 100k to make 50k to a pair of common points for front and rear stators. From the common points, connect the 0.0033uF to the sec ends of the SUT. The 0.0033uF plus 50k form a CR HPF. MAKE SURE the treble panel with its crossover is REVERSE PHASE CONNECTED TO THE BASS PANELS. The -3dB points in the signals in the electronic circuit thus created is 160Hz for bass, with signal rolling off at 6dB/octave above 160Hz, and 700Hz for the treble panels, also rolling off at 6dB/octave. Keeping pass signals out of the treble panel is a good idea. The speaker phase shift will be maximally quite large, but maybe under 60degrees, but I found the treble acoustic signal produced by the bass panels will affect the treble panel badly if not phase reversed ( like many other dynamic speakers ), and despite the attenuation by the R & C filter LPF effect of bass series R and the bass panel capacitance which totals 800pF. The ONLY way I could flatten the response and remove what was a wide 6dB dip in the resonse at 5kHz with reverse phase connections. This what I measured, and the acoustic response has little corelation to the signal applied. I will perhaps draw all the relevant curves of bass and treble signals applied and and include all this info at a website page. I hope to include a schematic of the equivalant LCR model of the the panels and SUT. I hope there would be a net positive result amoung builders of ESL. This should all have a very positive effect on understanding of what is really involved to make a pair of ESL speakers. Hopefully, all of what i say will fertilize the minds who created the ER Audio ESL speakers. They can scream long and hard at my critique, and i don't give a ****, their marketing is quite deceptive, and they say it'll be easy, and take only so long, but no, its not true, and they are bull****ting, and the total time I will end up spending on R&D, and patching up the mess of the thing they supplied plus do all the woodwork will amount to 10 times the time they say. My customer here was lulled into the project, along with me, under what now seem like false statements about the product. Had I known of all the difficulties and parts quality and non inclusions, i would never ever have agreed to my building of one of these kits after my customer bought it. He isn't technically minded, and could NEVER EVER have successfully built a kit from ERA. If I allowed quite low trade rates of $50 per hour to build these speakers and fix problems and do R&D, I would find I would be entitled to claim a payment of maybe $5,000 for the labour of building these speakers, plus the cost of supply of items not included, about $400. being a gentleman I won't ask more than a fraction of the figure from my customer, but frankly, the sooner I see these speakers leaving my workshop, the better, and I don't ever want to build another pair that I did not fully design myself!!!!! The original kit price was $2,000, and so the whole deal of up $7,400 value is quite poor value when a fully restored/rebuilt pair of Quad ESL57 could be had for about $4,000 from one John Hall in Melbourne. I have a Quad ESL57 which is unrestored and it even outperforms the ERA on most counts. How anyone could say the ERA speaker is better product than a Quad ESL57 or ESL63, as some have suggested is quite beyond me; maybe these people had old speakers with lots of faults, and replaced them with ERA because they thought they'd be better. The other complaint I have about the ESL3B is that its ONE panel, not two bass with one treble, like ESL2B. This means that if a membrane tears or ****s up in just one of the 3 sub panels, the WHOLE 3 subpanels have to be fixed, rather than just fix one of the 3 sub panels. There is BS spiel about why the ESL3B is a better than others, but ERA are pushing the flat ESL3B because it appears to me the cost of production is less for the less complex product. but the repair bills for YOU, the buyer, will always be higher. All the comparisons one reads make silly one liner statements without the pages of detailed back ups. So don't make me waste more time reading your replies which are not backed up with facts. Patrick Turner. **** me..!!?? Shouldn't you be out on your bike somewhere...?? |
ER Audio ESL-3B speaker kit progress, 22 May07.
"Keith G" wrote in message ... "Patrick Turner" wrote in message ... Some of you may have been following my reported progress with trying to build a pair of ER Audio ESL-IIIB kits which were purchased by a customer of mine from http://www.eraudio.com.au/index.html I have had the job of "assembling" these kits to a satisfactory level of operation. I got started back in about February this year and could not proceed as quickly as planned because of difficulties encountered resulting from the poor design of the kits. Before people think I have no prowess at building kits or speakers or amplifiers, just take a look at my website at http://www.turneraudio.com.au and compare the amount of information and depth of understanding compared with the all too brief techno info at the ER Audio site. At the ER site there is no proper electronic schematic for the ESL3B as it should be, no impedance measurements, and no measured performance data. These should be stated with ESL, because some amps will NOT be able to drive the ER speakers, whereas the speakers at my site are all easily drivable, and everyone knows about SEAS drivers being OK, so nothing I have made is any worse than the best speakers made with SEAS drivers such as Sonus Faber and Vienna Acoustic. I gurantee a flat full range response, ER don't gurantee anything. I have now overcome most of the ERA problems; I was not warned by anything at the ER Audio site. Here is the history so far of what happened, and it includes process details and some solutions worth remembering. The kit was supplied with spacers already glued to the 1,200mm x 550mm frames for the 3 panel speaker. 8 of the 12 machine screws riveted to the 12 stator plates were too long, and I had to cut them down with a Dremel tool to 6mm. Failure to notice if the screws are too long will result in a completely stuffed panel, because the stators frames won't press down flat properly onto the frames they are glued into with polyurethane glue. The only real mistake I made was with the first attempt to stretch a membrane of the 3.5uM gossamer thin mylar membrane. It is just so delicate! It was easy to tear using tape and a spring balance for sequential tensioning. And sure enough it tore, and I had to begin again, and the second attempt went perfectly until I glued the first frame with its stators in place onto the surface of the stretched out membrane using super glue. Unfortunately, a pin hole of invisible size allowed super glue to seep through to the bench underneath, and the membrane was ruined as I lifted the panel off the bench. Its easy to sand it off the frame and clean up to do it again. Could practice make perfect? I was about to learn.... Use of superglue as recommended in the ERA 33 pages of kit instructions was abandoned!!! I sanded down the surface of the MDF sheet I was using as the bench top with very fine 600 grade wet and dry sandpaper to remove whatever might have caused a damn pinhole. The bench sits on top of a heavy oak dining table I built 31 years ago from thick oak planks. ( I don't have dinner parties anymore, and the accoutrements of a gentleman have more productive uses these days ) The third membrane went fine when I stretched it, and I used the polyurethane glue to glue to the frame after painting on the glue thinly to the plastic frame. I learnt that the easiest way to weigh down the frame on top of the membrane already stretched out on the perfectly flat solid bench is with about 24 house bricks. After lowering the frame with wet glue onto the membrane, cover the frame with a damp towel. The moisture in the towel will ensure the polyurethane glue cures well in 24 hours. Place the bricks on top of the towel gently without allowing the frame to slide around. When all bricks are placed, gently go to each prick and press down hard with about 20Kg in turn, and this will help remove air bubbles in the glue. The towel prevents brick particles falling into the speaker panel. You need to be very clean about everything with the construction; I used my loungeroom because of the good lights, and clean environment. Next day I very carefully cut around the edge of the membrane and I had a perfect looking membrane when I lifted the bricks and towel away and lifted the frame. The conductive strip of copper foil was placed on the second frame and there were no problems. This self adhesive strip 4.5m wide by about 0.2mm thick is actually the foil they use around bits of glass used in leadlighting windows, and is easily available. DON'T drill the 4.5mm dia holes for the 12 x 4mm dia plastic bolts too close to spacer edges or else the membrane will not glue to the spacer properly and will begin a tear at the hole. If you don't understand this, you will have torn membranes, and need to relocate bolt holes, after filling up wrong ones, and this is a PITA..... I applied the high resistance coating to the membrane. All seemed to go OK but I used twice more than recomended, and Rob Mackinlay from ER later said I shouldn't use too much. After waiting a week for the coating to cure, I completed the basic assembly with supplied plastic bolts and plastic surrounds and I had a basically completed speaker, but without the timber surround or box for electronics underneath. The kit does not include any surround timber frame or box, and one is left to make all that oneself, its rather like being given a speaker kit with drivers but without a box. I can only imagine the terrible attempts being made by amateur audiophiles who have no carpentry or joinery making skills or tools. You won't want to see their speakers pictured on the Web. Then came time to hook up the input transformer and build the not supplied board for a suitable cross over for the speakers. I designed and built the un-supplied crossover and required board. The electronic parts supplied were a regulated LV dc power supply which can be adjusted for its dc level. This then feeds a supplied EHT supply which converts the sub 10Vdc to up to about -5.5kV for application to the membrane. The EHT supply is connected with -EHT voltage taken to the copper foil strip around the frames and the ground terminal of the EHT supply is taken to the CT of the SUT secondary. The SUT is supplied, but has half the core size and half the primary turns really needed for saturation proof operation. I have advised ER Audio with full details of an alternative design for their transformer, and i look forward to them addopting my recomendations. The supplied SUT has far too thin P to S insulation, resulting in 390pF of shunt capacitance appearing across the secondary, which transforms to massive 3.16uF at the primary. The treble panel has 100pF capacitance which transforms to 0.81uF, and the total input capacitance seen by the amplifier = 4uF, ( about twice what Quad ESL57 managed ). The bass panel capacitance of 800pF transforms to 6.5uF at the primary, but the series resistance prevents this much C ever being experienced as a load on the amp, so bass panel C is quite entirely benign. I tried a very basic crossover network about which I will have more to say, and hooked up the speaker and tranny to an amplifier capable of 21Vrms max into a high Z load, and up to 70 watts into 3 ohms, 14.5Vrms. Output Z was 0.2 ohms, BW 7Hz to 30kHz, 2 ohms connected at low levels, and THD 0.2% at max po into 8 ohms, 50 watts, 18Vrms, and mainly class A with a quad of mosfets. I turned on the EHT and gradually increased the EHT until I heard all kinds of spluttery spittery sounds and saw numerous blue discharges occuring all over the panels. I backed off immediately until the noises stopped and conducted sound tests using pink noise and test gear as described in my speaker building pages at http://www.turneraudio.com.au/loudspeakers-diy.html Then I began testing the responses at 1M, 2M ,4M distances at a 1.2M off floor level, on axis, with the speaker taped temporarily to a stout dining chair I also built 31 years ago. Bottom of the speaker is 450mm above the floor, speaker is vertical. I got a truly appalling response. The sensitivity seemed appallingly low. For the same quite low level of pink noise, I needed maybe 5 times the voltage I'd need for my own Sublimes shown at http://www.turneraudio.com.au/loudspeakers-new.html The power handling was atrocious, and LF capablity suffered from arcing and distortions. My customer visted me in the middle of testing and was not impressed at all. We talked about quitting, but I ain't no bloody quitter. I obtained the loan of a high impedance HV probe to measure up to 20kV safely, and found that any EHT increase above 2.2kV cause horrid discharge noise and premature clipping. ESL sensitivity is about proportional to applied EHT voltage, and I wanted to be able to apply 5,000V if possible, like ESL57 and ESL63. I then thought that the arcing seen must be because the poor insulation qualities of the black powder coating on the suplied stators. So I stripped off membrane No 3, and coated all the stators with two generous coats of anti corona paint, Isonel 642, and put on a new membrane No 4 but with two very thin conductive coats on the membrane, this time using the right total amount and to get an even coating. I also placed in the pattern of 10 anti resonance silicone pads but that made no difference to following results. I re-tested after the rebuild and curing times, and although there was not such a lot of arcing and EHT leakage, the response and problems were quite unacceptable. I turned off the EHT supply, and considered using more membrane tension of 2Kg / 60mm of side length, not the low 0.8Kg recommended. ESL63 use 2.5Kg for the same material. Lots of crackling noises continued for minutes after turn off of the EHT and after the voltage had rapidly fallen to 0V. It was the membrane partially releasing from its stuck position. When I unbolted the two halves of the speaker the next day after the dismal tests, I found that about 70% of the area of both bass membranes had become glued to the stators on the side away from that where the membrane is coated. I was able to gently prise the membrane off the starors with a bit of bent copper wire poked through slots in the stators. Anti corona paint is slightly sticky with mylar. No wonder I had such horrible test results. But it had taken two attempts before I became aware of the problem and I guess that EVERY SILLY MAN WHO TRIES TO USE ABOVE ABOUT 3KV will have what I call membrane "stiction" problems. There are posts I've seen in these silly little private forums where they all bull**** to each other of guys cranking up the EHT and I believe they don't realize their problems. With stuck membranes, the speakers still work at mid & treble, but poorly, and definitely not as intended, and with queer bass. Back to my drawing board I went, and at this point I didn't think it would be wise to consult ER Audio for advice, and I posted on these groups to see if anyone else had had problems. One Collin Topps of the UK answered my initial posts to groups in private emails which began cordially, but ended rudely. Collin is the UK ERA sales rep. He said repeatedly nobody has had any problems building ER Audio panels. He refused to accept that I was having serious bothers, or offer any advice that was relevant and useful. Then he ended up telling me to sod off, and I thought that this technically dumb salesman in the UK acting for ER Audio as their sales agent has some basic things about public relations he has yet to learn. He'd sure never get a job selling anything I made. I continued to post on the panels and learn more about ESL construction from other ESL amateur productions around the world. Since then, I decided that the membrane must not be allowed to travel too close to a stator, ideally not more than half the actual distance between membrane and stator surface, so if this is 4mm, as it is in ESL57 bass panels, then 2mm is enough maximum movement distance. Quad achive this by using 2mm thick PVC plastic sheeting for bass stators, with conductive stator material being conductiove paint on the outside of the perforated plastic sheeting. So the membrane CANNOT move more than 2mm and cannot be less than 2mm away from the stator surface. The of force of electrostatic attraction increases proportionally to 1/d squared, so if d is only a few thousanths of an inch, F becomes huge. No wonder my ERA membranes were sticking like cling wrap around a pumpkin at the grocer. The bass panel membrane to stator distance in ERA panels is 2.4mm. I thought that if I applied about 0.8mm of non conductive material to the inside surface of the stator, It would keep the membrane getting too close to a stator, and the extra tension would always overcome the force caused by the EHT without signal. I'd have 1.6mm for membrane movement, not as much as in a Quad speaker, but enough. So I applied four coats of silicone paint made from roof and gutter silicone sealant bought for $5 per tube at a plumber's store. To coat all the stators for one speaker I used 1.3 tubes of silicone, and about 600ml of white spirit for thinning. The thinning is done by using a small cheap brush with dabbing action in a clean tuna fish can until the paint has thick honey consistency and no visible lumps. The silicone is applied by dabbing action with the brush laid flat on the perforated steel sheeting, not letting silicone close off perforation holes. It self levels fairly well, and partially wraps around the sharp metal edges of the holes in the stators, so probably enhances air flow caused by sound waves. 24 hours is fine between coats of silicone. It sticks well to the anti corona paint I already have on the stators. The silicone becomes rubbery, and smooth surfaced, even though some uneveness of this coating thickness occurs, but basically, I got the right amount of goop applied to all stator surfaces. I finally stretched membrane No 5 last week and have re-assembled the speaker for a new test. After the frame was first glued to the stretched and much tighter membrane, I still found the membrane tended to stick to the stator if pressed over to it gently by hand. So I then bought a small can of Johnson's Baby Powder and squirted in a lot of powder through perforations, and with an air blower, blew it all around everywhere. Then i sucked off the excess woth a gentle vacuum cleaner. On the opposite second frame and stators, i just dusted the powder on and removed excess with vacuum. The panel was then re-assembled. Did my ingenuity prevent the problems I was having? After connection of the speaker to the amp and without signal, I raised the EHT and at 3.2kV while I watched the bass membranes carefully I saw them whip over to a stator and remain hard against it. Hmm, same old problem. However, when i reduced EHT, the membrane let go without all the crackling sounds they'd made previously after turn off of the EHT supply. The powdered layer of rubber was doing the right kind of trick in preventing stiction. I was able to leave the EHT on all night at 3kV, but just occasionally, some small click noise would occur, so i have settled on having 2.7kV as the maximum EHT voltage which could be safely applied to these panels before problems would occur. I began to seriously test the speaker response and do serious comparisons again with my own blameless Sublimes. They sit side by side, and comparisons can be fairly made, same room, 200Cubic metres, well out from a wall, well damped etc. The same amps, test signal, test gear and mic is used to eliminate any chance of making an unfair comparison. Finally, I got the speakers to measure +/- 2dB between LF pole = 35Hz and HF pole = 22kHz, and to give as flat a response as I could get without adding a ridiculous number of crossover compensation networks. This response was measured at 3M with mic 800mm above the floor, and about exactly how they will be listened to in my customer's room, which is not quite as good as my own, but measurement of his existing speaker response has been little different to what i get in my rooms. If I get speakers to sound well here, they always travel well. My impressions with the sound with music is good, but the 50 watt class A amps I have been using for trials run completely out of headroom at only modest levels equal to about 1/3 watt average into my Sublimes which are 5.6 ohms average, and have 88dB/W/M watt sensitivity. After numerous calculations, I figured I needed 5 times the applied voltage for the same SPL with ERA panels compared to my own speakers. At least a 100 watt amp would be needed for quite modest levels of sound, not because 100 watts would ever be generated, but merely to get enough voltage. Collin Tops said he was using an SET amp with 16 watts only, and maybe he likes quietspeakers. But I prefer loudspeakers. And for these ERA quietspeakers, there is not the slightest bit of speaker protection circuitry included as it is in Quad ESL63. What is the safe maximum voltage? not as much as for Quads, that's for sure. Anyway, I did clip the 50 watt amp a few times when i tried to go loud with some busy Salsa music from Buena Vista Social Club, and nothing bad happened, so the 6 coats of goop I have on the stators seemes to resist arcing. A 16 watt SET amp with Rout 2ohms would be a horrible thing to drive such ESL. There would be a serious HF roll off, but perhaps Collin is an old giza with stuffed hearing, and so may not mind if the HF pole = 6kHz. And without my networks and crossovers, the response could be worse, peaked up high between 500 and 6kHz, ie, without bass or treble. He will have to conduct all the same well conducted tests i have done before he'd ever know WTF he's actually built. He should not be offended when I say I don't trust what salesmen tell me. Nobody from ERA has had the courage to discuss their speakers in the public forums. I have just measured the Z, and with the details of networks below got the following Z figures:- 10Hz, approx 80ohms, 20Hz, 41, 50Hz, 14, 60Hz, 11, 80Hz, 10, 110Hz, 11, 200Hz, 18, 300Hz, 20, 500Hz, 19, 1kHz, 15, 2kHz, 11.5, 10kHz, 5, 20kHz, 3, 40kHz, 2. If you plot the above points on a graphed sheet of log paper, and join the dots with gentle curves and you will have the Z. The average Z between 50Hz and 2kHz = 14 ohms. Therefore a tube amp set up for a match to 16 ohms will work, but it'd need to be able to make 30Vrms, which is 64 watts into 14 ohms. The amount of signal above 2kHz which feeds the low Z average of 5ohms between 2khz and 20kHz is small, and as long as the Rout 0.5 ohms there will not be a serious loss of HF detail. One of my 8585 tube amplifiers with a quad of KT90 in PP per channel is powering 3 stacked pairs of ESL57 no problems, even though the Z = 0.6 ohms at 18kHz. But 16 watts from SET would be hopless, unless you had the speakers so close they are like giant ESL headphones. DO NOT use the recommended circuit resistances so vaguely shown in the ER instructions. I found that the best way to hook up the ESL-3B speakers is as follows:- BEFORE the the input to the primary of the step up transformer, ( SUT ):- Make a series L + R network of 4mH plus 27 ohms. Connect this across the P winding. Connect one end of the P winding to the 0V terminal for the black lead from the amplifier. To the other live primary end, connect a series C & R network of 150uF plus 1.5ohms across to the speaker terminal to which the red wire from the amp connects. These two input networks will have several effects. The 27 ohms plus 4mH makes the input loaded with 27 ohms at low F, thus damping the low Z of the series 150uF and primary shunt inductance of 32 mH. The 150uF will prevent LF entering the speaker and causing the rather poor quality SUT from saturating all too easily with high transient LF voltages. The -3dB cut off is at 50Hz, and the attenuation is second order, barely enough. To get better headroom for these speakers, use a second input cap in series of 100uF, giving -3db at about 100Hz, then use a sub. More signal will be then applicable above 100Hz. The 1.5 ohms adds to the 0.5 ohms of SUT winding resistance which is important to damp the series resonance between the awfully high amount of shunt capacitance in the SUT and the leakage inductance at around 20kHz. Therefore input resistance is a minimum of 2ohms by 50kHz, so not many amps should blow up. AFTER the secondary of the SUT, place the following networks from each end of sec to the bass panel terminals:- You will need the following parts, 16 x 100k resistors, metal film, 1%, 2 watt rated. 2 x 0.0033uF capacitors rated at 4kV. Find good quality polypropylene caps. To each bass stator, connect 100k to a pair of common points for the rear and front pairs of bass panels, Then series 4 x 100k to make 400k from each common point to the ends of the SUT secondary. To each treble stator, connect a parallel pair of 100k to make 50k to a pair of common points for front and rear stators. From the common points, connect the 0.0033uF to the sec ends of the SUT. The 0.0033uF plus 50k form a CR HPF. MAKE SURE the treble panel with its crossover is REVERSE PHASE CONNECTED TO THE BASS PANELS. The -3dB points in the signals in the electronic circuit thus created is 160Hz for bass, with signal rolling off at 6dB/octave above 160Hz, and 700Hz for the treble panels, also rolling off at 6dB/octave. Keeping pass signals out of the treble panel is a good idea. The speaker phase shift will be maximally quite large, but maybe under 60degrees, but I found the treble acoustic signal produced by the bass panels will affect the treble panel badly if not phase reversed ( like many other dynamic speakers ), and despite the attenuation by the R & C filter LPF effect of bass series R and the bass panel capacitance which totals 800pF. The ONLY way I could flatten the response and remove what was a wide 6dB dip in the resonse at 5kHz with reverse phase connections. This what I measured, and the acoustic response has little corelation to the signal applied. I will perhaps draw all the relevant curves of bass and treble signals applied and and include all this info at a website page. I hope to include a schematic of the equivalant LCR model of the the panels and SUT. I hope there would be a net positive result amoung builders of ESL. This should all have a very positive effect on understanding of what is really involved to make a pair of ESL speakers. Hopefully, all of what i say will fertilize the minds who created the ER Audio ESL speakers. They can scream long and hard at my critique, and i don't give a ****, their marketing is quite deceptive, and they say it'll be easy, and take only so long, but no, its not true, and they are bull****ting, and the total time I will end up spending on R&D, and patching up the mess of the thing they supplied plus do all the woodwork will amount to 10 times the time they say. My customer here was lulled into the project, along with me, under what now seem like false statements about the product. Had I known of all the difficulties and parts quality and non inclusions, i would never ever have agreed to my building of one of these kits after my customer bought it. He isn't technically minded, and could NEVER EVER have successfully built a kit from ERA. If I allowed quite low trade rates of $50 per hour to build these speakers and fix problems and do R&D, I would find I would be entitled to claim a payment of maybe $5,000 for the labour of building these speakers, plus the cost of supply of items not included, about $400. being a gentleman I won't ask more than a fraction of the figure from my customer, but frankly, the sooner I see these speakers leaving my workshop, the better, and I don't ever want to build another pair that I did not fully design myself!!!!! The original kit price was $2,000, and so the whole deal of up $7,400 value is quite poor value when a fully restored/rebuilt pair of Quad ESL57 could be had for about $4,000 from one John Hall in Melbourne. I have a Quad ESL57 which is unrestored and it even outperforms the ERA on most counts. How anyone could say the ERA speaker is better product than a Quad ESL57 or ESL63, as some have suggested is quite beyond me; maybe these people had old speakers with lots of faults, and replaced them with ERA because they thought they'd be better. The other complaint I have about the ESL3B is that its ONE panel, not two bass with one treble, like ESL2B. This means that if a membrane tears or ****s up in just one of the 3 sub panels, the WHOLE 3 subpanels have to be fixed, rather than just fix one of the 3 sub panels. There is BS spiel about why the ESL3B is a better than others, but ERA are pushing the flat ESL3B because it appears to me the cost of production is less for the less complex product. but the repair bills for YOU, the buyer, will always be higher. All the comparisons one reads make silly one liner statements without the pages of detailed back ups. So don't make me waste more time reading your replies which are not backed up with facts. Patrick Turner. **** me..!!?? Shouldn't you be out on your bike somewhere...?? Well that's me total stuffed, and I ordered 12 house bricks from Bunning's, special. Just perhaps you need to be a total moron to build, construct, make, assemble such rubbish, and not someone who considers themselves technically perfect. A little knowledge can be a very dangerous thing.. So next time you get something like this to assemble, Bung it over to me, it sounds like a job for a wet weekend. So who got a solid 12 seater Dinner table to lend me.. Frankly all your technical mumbo-jumbo doesn't count for ****, if the things sound like crap on completion Even if they are an example of technically perfection. Frankly, I can't understand why anyone would bother with a kit, When the real "warranty" things can be obtained without having a compulsory nervous breakdown. bassett |
ER Audio ESL-3B speaker kit progress, 22 May07.
"Keith G" wrote in message ... "Patrick Turner" wrote in message ... Some of you may have been following my reported progress with trying to build a pair of ER Audio ESL-IIIB kits which were purchased by a customer of mine from http://www.eraudio.com.au/index.html I have had the job of "assembling" these kits to a satisfactory level of operation. I got started back in about February this year and could not proceed as quickly as planned because of difficulties encountered resulting from the poor design of the kits. Before people think I have no prowess at building kits or speakers or amplifiers, just take a look at my website at http://www.turneraudio.com.au and compare the amount of information and depth of understanding compared with the all too brief techno info at the ER Audio site. At the ER site there is no proper electronic schematic for the ESL3B as it should be, no impedance measurements, and no measured performance data. These should be stated with ESL, because some amps will NOT be able to drive the ER speakers, whereas the speakers at my site are all easily drivable, and everyone knows about SEAS drivers being OK, so nothing I have made is any worse than the best speakers made with SEAS drivers such as Sonus Faber and Vienna Acoustic. I gurantee a flat full range response, ER don't gurantee anything. I have now overcome most of the ERA problems; I was not warned by anything at the ER Audio site. Here is the history so far of what happened, and it includes process details and some solutions worth remembering. The kit was supplied with spacers already glued to the 1,200mm x 550mm frames for the 3 panel speaker. 8 of the 12 machine screws riveted to the 12 stator plates were too long, and I had to cut them down with a Dremel tool to 6mm. Failure to notice if the screws are too long will result in a completely stuffed panel, because the stators frames won't press down flat properly onto the frames they are glued into with polyurethane glue. The only real mistake I made was with the first attempt to stretch a membrane of the 3.5uM gossamer thin mylar membrane. It is just so delicate! It was easy to tear using tape and a spring balance for sequential tensioning. And sure enough it tore, and I had to begin again, and the second attempt went perfectly until I glued the first frame with its stators in place onto the surface of the stretched out membrane using super glue. Unfortunately, a pin hole of invisible size allowed super glue to seep through to the bench underneath, and the membrane was ruined as I lifted the panel off the bench. Its easy to sand it off the frame and clean up to do it again. Could practice make perfect? I was about to learn.... Use of superglue as recommended in the ERA 33 pages of kit instructions was abandoned!!! I sanded down the surface of the MDF sheet I was using as the bench top with very fine 600 grade wet and dry sandpaper to remove whatever might have caused a damn pinhole. The bench sits on top of a heavy oak dining table I built 31 years ago from thick oak planks. ( I don't have dinner parties anymore, and the accoutrements of a gentleman have more productive uses these days ) The third membrane went fine when I stretched it, and I used the polyurethane glue to glue to the frame after painting on the glue thinly to the plastic frame. I learnt that the easiest way to weigh down the frame on top of the membrane already stretched out on the perfectly flat solid bench is with about 24 house bricks. After lowering the frame with wet glue onto the membrane, cover the frame with a damp towel. The moisture in the towel will ensure the polyurethane glue cures well in 24 hours. Place the bricks on top of the towel gently without allowing the frame to slide around. When all bricks are placed, gently go to each prick and press down hard with about 20Kg in turn, and this will help remove air bubbles in the glue. The towel prevents brick particles falling into the speaker panel. You need to be very clean about everything with the construction; I used my loungeroom because of the good lights, and clean environment. Next day I very carefully cut around the edge of the membrane and I had a perfect looking membrane when I lifted the bricks and towel away and lifted the frame. The conductive strip of copper foil was placed on the second frame and there were no problems. This self adhesive strip 4.5m wide by about 0.2mm thick is actually the foil they use around bits of glass used in leadlighting windows, and is easily available. DON'T drill the 4.5mm dia holes for the 12 x 4mm dia plastic bolts too close to spacer edges or else the membrane will not glue to the spacer properly and will begin a tear at the hole. If you don't understand this, you will have torn membranes, and need to relocate bolt holes, after filling up wrong ones, and this is a PITA..... I applied the high resistance coating to the membrane. All seemed to go OK but I used twice more than recomended, and Rob Mackinlay from ER later said I shouldn't use too much. After waiting a week for the coating to cure, I completed the basic assembly with supplied plastic bolts and plastic surrounds and I had a basically completed speaker, but without the timber surround or box for electronics underneath. The kit does not include any surround timber frame or box, and one is left to make all that oneself, its rather like being given a speaker kit with drivers but without a box. I can only imagine the terrible attempts being made by amateur audiophiles who have no carpentry or joinery making skills or tools. You won't want to see their speakers pictured on the Web. Then came time to hook up the input transformer and build the not supplied board for a suitable cross over for the speakers. I designed and built the un-supplied crossover and required board. The electronic parts supplied were a regulated LV dc power supply which can be adjusted for its dc level. This then feeds a supplied EHT supply which converts the sub 10Vdc to up to about -5.5kV for application to the membrane. The EHT supply is connected with -EHT voltage taken to the copper foil strip around the frames and the ground terminal of the EHT supply is taken to the CT of the SUT secondary. The SUT is supplied, but has half the core size and half the primary turns really needed for saturation proof operation. I have advised ER Audio with full details of an alternative design for their transformer, and i look forward to them addopting my recomendations. The supplied SUT has far too thin P to S insulation, resulting in 390pF of shunt capacitance appearing across the secondary, which transforms to massive 3.16uF at the primary. The treble panel has 100pF capacitance which transforms to 0.81uF, and the total input capacitance seen by the amplifier = 4uF, ( about twice what Quad ESL57 managed ). The bass panel capacitance of 800pF transforms to 6.5uF at the primary, but the series resistance prevents this much C ever being experienced as a load on the amp, so bass panel C is quite entirely benign. I tried a very basic crossover network about which I will have more to say, and hooked up the speaker and tranny to an amplifier capable of 21Vrms max into a high Z load, and up to 70 watts into 3 ohms, 14.5Vrms. Output Z was 0.2 ohms, BW 7Hz to 30kHz, 2 ohms connected at low levels, and THD 0.2% at max po into 8 ohms, 50 watts, 18Vrms, and mainly class A with a quad of mosfets. I turned on the EHT and gradually increased the EHT until I heard all kinds of spluttery spittery sounds and saw numerous blue discharges occuring all over the panels. I backed off immediately until the noises stopped and conducted sound tests using pink noise and test gear as described in my speaker building pages at http://www.turneraudio.com.au/loudspeakers-diy.html Then I began testing the responses at 1M, 2M ,4M distances at a 1.2M off floor level, on axis, with the speaker taped temporarily to a stout dining chair I also built 31 years ago. Bottom of the speaker is 450mm above the floor, speaker is vertical. I got a truly appalling response. The sensitivity seemed appallingly low. For the same quite low level of pink noise, I needed maybe 5 times the voltage I'd need for my own Sublimes shown at http://www.turneraudio.com.au/loudspeakers-new.html The power handling was atrocious, and LF capablity suffered from arcing and distortions. My customer visted me in the middle of testing and was not impressed at all. We talked about quitting, but I ain't no bloody quitter. I obtained the loan of a high impedance HV probe to measure up to 20kV safely, and found that any EHT increase above 2.2kV cause horrid discharge noise and premature clipping. ESL sensitivity is about proportional to applied EHT voltage, and I wanted to be able to apply 5,000V if possible, like ESL57 and ESL63. I then thought that the arcing seen must be because the poor insulation qualities of the black powder coating on the suplied stators. So I stripped off membrane No 3, and coated all the stators with two generous coats of anti corona paint, Isonel 642, and put on a new membrane No 4 but with two very thin conductive coats on the membrane, this time using the right total amount and to get an even coating. I also placed in the pattern of 10 anti resonance silicone pads but that made no difference to following results. I re-tested after the rebuild and curing times, and although there was not such a lot of arcing and EHT leakage, the response and problems were quite unacceptable. I turned off the EHT supply, and considered using more membrane tension of 2Kg / 60mm of side length, not the low 0.8Kg recommended. ESL63 use 2.5Kg for the same material. Lots of crackling noises continued for minutes after turn off of the EHT and after the voltage had rapidly fallen to 0V. It was the membrane partially releasing from its stuck position. When I unbolted the two halves of the speaker the next day after the dismal tests, I found that about 70% of the area of both bass membranes had become glued to the stators on the side away from that where the membrane is coated. I was able to gently prise the membrane off the starors with a bit of bent copper wire poked through slots in the stators. Anti corona paint is slightly sticky with mylar. No wonder I had such horrible test results. But it had taken two attempts before I became aware of the problem and I guess that EVERY SILLY MAN WHO TRIES TO USE ABOVE ABOUT 3KV will have what I call membrane "stiction" problems. There are posts I've seen in these silly little private forums where they all bull**** to each other of guys cranking up the EHT and I believe they don't realize their problems. With stuck membranes, the speakers still work at mid & treble, but poorly, and definitely not as intended, and with queer bass. Back to my drawing board I went, and at this point I didn't think it would be wise to consult ER Audio for advice, and I posted on these groups to see if anyone else had had problems. One Collin Topps of the UK answered my initial posts to groups in private emails which began cordially, but ended rudely. Collin is the UK ERA sales rep. He said repeatedly nobody has had any problems building ER Audio panels. He refused to accept that I was having serious bothers, or offer any advice that was relevant and useful. Then he ended up telling me to sod off, and I thought that this technically dumb salesman in the UK acting for ER Audio as their sales agent has some basic things about public relations he has yet to learn. He'd sure never get a job selling anything I made. I continued to post on the panels and learn more about ESL construction from other ESL amateur productions around the world. Since then, I decided that the membrane must not be allowed to travel too close to a stator, ideally not more than half the actual distance between membrane and stator surface, so if this is 4mm, as it is in ESL57 bass panels, then 2mm is enough maximum movement distance. Quad achive this by using 2mm thick PVC plastic sheeting for bass stators, with conductive stator material being conductiove paint on the outside of the perforated plastic sheeting. So the membrane CANNOT move more than 2mm and cannot be less than 2mm away from the stator surface. The of force of electrostatic attraction increases proportionally to 1/d squared, so if d is only a few thousanths of an inch, F becomes huge. No wonder my ERA membranes were sticking like cling wrap around a pumpkin at the grocer. The bass panel membrane to stator distance in ERA panels is 2.4mm. I thought that if I applied about 0.8mm of non conductive material to the inside surface of the stator, It would keep the membrane getting too close to a stator, and the extra tension would always overcome the force caused by the EHT without signal. I'd have 1.6mm for membrane movement, not as much as in a Quad speaker, but enough. So I applied four coats of silicone paint made from roof and gutter silicone sealant bought for $5 per tube at a plumber's store. To coat all the stators for one speaker I used 1.3 tubes of silicone, and about 600ml of white spirit for thinning. The thinning is done by using a small cheap brush with dabbing action in a clean tuna fish can until the paint has thick honey consistency and no visible lumps. The silicone is applied by dabbing action with the brush laid flat on the perforated steel sheeting, not letting silicone close off perforation holes. It self levels fairly well, and partially wraps around the sharp metal edges of the holes in the stators, so probably enhances air flow caused by sound waves. 24 hours is fine between coats of silicone. It sticks well to the anti corona paint I already have on the stators. The silicone becomes rubbery, and smooth surfaced, even though some uneveness of this coating thickness occurs, but basically, I got the right amount of goop applied to all stator surfaces. I finally stretched membrane No 5 last week and have re-assembled the speaker for a new test. After the frame was first glued to the stretched and much tighter membrane, I still found the membrane tended to stick to the stator if pressed over to it gently by hand. So I then bought a small can of Johnson's Baby Powder and squirted in a lot of powder through perforations, and with an air blower, blew it all around everywhere. Then i sucked off the excess woth a gentle vacuum cleaner. On the opposite second frame and stators, i just dusted the powder on and removed excess with vacuum. The panel was then re-assembled. Did my ingenuity prevent the problems I was having? After connection of the speaker to the amp and without signal, I raised the EHT and at 3.2kV while I watched the bass membranes carefully I saw them whip over to a stator and remain hard against it. Hmm, same old problem. However, when i reduced EHT, the membrane let go without all the crackling sounds they'd made previously after turn off of the EHT supply. The powdered layer of rubber was doing the right kind of trick in preventing stiction. I was able to leave the EHT on all night at 3kV, but just occasionally, some small click noise would occur, so i have settled on having 2.7kV as the maximum EHT voltage which could be safely applied to these panels before problems would occur. I began to seriously test the speaker response and do serious comparisons again with my own blameless Sublimes. They sit side by side, and comparisons can be fairly made, same room, 200Cubic metres, well out from a wall, well damped etc. The same amps, test signal, test gear and mic is used to eliminate any chance of making an unfair comparison. Finally, I got the speakers to measure +/- 2dB between LF pole = 35Hz and HF pole = 22kHz, and to give as flat a response as I could get without adding a ridiculous number of crossover compensation networks. This response was measured at 3M with mic 800mm above the floor, and about exactly how they will be listened to in my customer's room, which is not quite as good as my own, but measurement of his existing speaker response has been little different to what i get in my rooms. If I get speakers to sound well here, they always travel well. My impressions with the sound with music is good, but the 50 watt class A amps I have been using for trials run completely out of headroom at only modest levels equal to about 1/3 watt average into my Sublimes which are 5.6 ohms average, and have 88dB/W/M watt sensitivity. After numerous calculations, I figured I needed 5 times the applied voltage for the same SPL with ERA panels compared to my own speakers. At least a 100 watt amp would be needed for quite modest levels of sound, not because 100 watts would ever be generated, but merely to get enough voltage. Collin Tops said he was using an SET amp with 16 watts only, and maybe he likes quietspeakers. But I prefer loudspeakers. And for these ERA quietspeakers, there is not the slightest bit of speaker protection circuitry included as it is in Quad ESL63. What is the safe maximum voltage? not as much as for Quads, that's for sure. Anyway, I did clip the 50 watt amp a few times when i tried to go loud with some busy Salsa music from Buena Vista Social Club, and nothing bad happened, so the 6 coats of goop I have on the stators seemes to resist arcing. A 16 watt SET amp with Rout 2ohms would be a horrible thing to drive such ESL. There would be a serious HF roll off, but perhaps Collin is an old giza with stuffed hearing, and so may not mind if the HF pole = 6kHz. And without my networks and crossovers, the response could be worse, peaked up high between 500 and 6kHz, ie, without bass or treble. He will have to conduct all the same well conducted tests i have done before he'd ever know WTF he's actually built. He should not be offended when I say I don't trust what salesmen tell me. Nobody from ERA has had the courage to discuss their speakers in the public forums. I have just measured the Z, and with the details of networks below got the following Z figures:- 10Hz, approx 80ohms, 20Hz, 41, 50Hz, 14, 60Hz, 11, 80Hz, 10, 110Hz, 11, 200Hz, 18, 300Hz, 20, 500Hz, 19, 1kHz, 15, 2kHz, 11.5, 10kHz, 5, 20kHz, 3, 40kHz, 2. If you plot the above points on a graphed sheet of log paper, and join the dots with gentle curves and you will have the Z. The average Z between 50Hz and 2kHz = 14 ohms. Therefore a tube amp set up for a match to 16 ohms will work, but it'd need to be able to make 30Vrms, which is 64 watts into 14 ohms. The amount of signal above 2kHz which feeds the low Z average of 5ohms between 2khz and 20kHz is small, and as long as the Rout 0.5 ohms there will not be a serious loss of HF detail. One of my 8585 tube amplifiers with a quad of KT90 in PP per channel is powering 3 stacked pairs of ESL57 no problems, even though the Z = 0.6 ohms at 18kHz. But 16 watts from SET would be hopless, unless you had the speakers so close they are like giant ESL headphones. DO NOT use the recommended circuit resistances so vaguely shown in the ER instructions. I found that the best way to hook up the ESL-3B speakers is as follows:- BEFORE the the input to the primary of the step up transformer, ( SUT ):- Make a series L + R network of 4mH plus 27 ohms. Connect this across the P winding. Connect one end of the P winding to the 0V terminal for the black lead from the amplifier. To the other live primary end, connect a series C & R network of 150uF plus 1.5ohms across to the speaker terminal to which the red wire from the amp connects. These two input networks will have several effects. The 27 ohms plus 4mH makes the input loaded with 27 ohms at low F, thus damping the low Z of the series 150uF and primary shunt inductance of 32 mH. The 150uF will prevent LF entering the speaker and causing the rather poor quality SUT from saturating all too easily with high transient LF voltages. The -3dB cut off is at 50Hz, and the attenuation is second order, barely enough. To get better headroom for these speakers, use a second input cap in series of 100uF, giving -3db at about 100Hz, then use a sub. More signal will be then applicable above 100Hz. The 1.5 ohms adds to the 0.5 ohms of SUT winding resistance which is important to damp the series resonance between the awfully high amount of shunt capacitance in the SUT and the leakage inductance at around 20kHz. Therefore input resistance is a minimum of 2ohms by 50kHz, so not many amps should blow up. AFTER the secondary of the SUT, place the following networks from each end of sec to the bass panel terminals:- You will need the following parts, 16 x 100k resistors, metal film, 1%, 2 watt rated. 2 x 0.0033uF capacitors rated at 4kV. Find good quality polypropylene caps. To each bass stator, connect 100k to a pair of common points for the rear and front pairs of bass panels, Then series 4 x 100k to make 400k from each common point to the ends of the SUT secondary. To each treble stator, connect a parallel pair of 100k to make 50k to a pair of common points for front and rear stators. From the common points, connect the 0.0033uF to the sec ends of the SUT. The 0.0033uF plus 50k form a CR HPF. MAKE SURE the treble panel with its crossover is REVERSE PHASE CONNECTED TO THE BASS PANELS. The -3dB points in the signals in the electronic circuit thus created is 160Hz for bass, with signal rolling off at 6dB/octave above 160Hz, and 700Hz for the treble panels, also rolling off at 6dB/octave. Keeping pass signals out of the treble panel is a good idea. The speaker phase shift will be maximally quite large, but maybe under 60degrees, but I found the treble acoustic signal produced by the bass panels will affect the treble panel badly if not phase reversed ( like many other dynamic speakers ), and despite the attenuation by the R & C filter LPF effect of bass series R and the bass panel capacitance which totals 800pF. The ONLY way I could flatten the response and remove what was a wide 6dB dip in the resonse at 5kHz with reverse phase connections. This what I measured, and the acoustic response has little corelation to the signal applied. I will perhaps draw all the relevant curves of bass and treble signals applied and and include all this info at a website page. I hope to include a schematic of the equivalant LCR model of the the panels and SUT. I hope there would be a net positive result amoung builders of ESL. This should all have a very positive effect on understanding of what is really involved to make a pair of ESL speakers. Hopefully, all of what i say will fertilize the minds who created the ER Audio ESL speakers. They can scream long and hard at my critique, and i don't give a ****, their marketing is quite deceptive, and they say it'll be easy, and take only so long, but no, its not true, and they are bull****ting, and the total time I will end up spending on R&D, and patching up the mess of the thing they supplied plus do all the woodwork will amount to 10 times the time they say. My customer here was lulled into the project, along with me, under what now seem like false statements about the product. Had I known of all the difficulties and parts quality and non inclusions, i would never ever have agreed to my building of one of these kits after my customer bought it. He isn't technically minded, and could NEVER EVER have successfully built a kit from ERA. If I allowed quite low trade rates of $50 per hour to build these speakers and fix problems and do R&D, I would find I would be entitled to claim a payment of maybe $5,000 for the labour of building these speakers, plus the cost of supply of items not included, about $400. being a gentleman I won't ask more than a fraction of the figure from my customer, but frankly, the sooner I see these speakers leaving my workshop, the better, and I don't ever want to build another pair that I did not fully design myself!!!!! The original kit price was $2,000, and so the whole deal of up $7,400 value is quite poor value when a fully restored/rebuilt pair of Quad ESL57 could be had for about $4,000 from one John Hall in Melbourne. I have a Quad ESL57 which is unrestored and it even outperforms the ERA on most counts. How anyone could say the ERA speaker is better product than a Quad ESL57 or ESL63, as some have suggested is quite beyond me; maybe these people had old speakers with lots of faults, and replaced them with ERA because they thought they'd be better. The other complaint I have about the ESL3B is that its ONE panel, not two bass with one treble, like ESL2B. This means that if a membrane tears or ****s up in just one of the 3 sub panels, the WHOLE 3 subpanels have to be fixed, rather than just fix one of the 3 sub panels. There is BS spiel about why the ESL3B is a better than others, but ERA are pushing the flat ESL3B because it appears to me the cost of production is less for the less complex product. but the repair bills for YOU, the buyer, will always be higher. All the comparisons one reads make silly one liner statements without the pages of detailed back ups. So don't make me waste more time reading your replies which are not backed up with facts. Patrick Turner. **** me..!!?? Shouldn't you be out on your bike somewhere...?? ] Professor, What you described was a horror story for a layman. With all said and done, how do the bloody contraptions sound? west |
ER Audio ESL-3B speaker kit progress, 22 May07.
You have my deepest sympathies. This reminds me of some of the items
that have crossed my bench for repair where the owner has a sentimental reason or some such that makes even the most irrational approach feasible. One such case, I actually took the few useable parts out of the item (one output transformer, a choke, front panel and knobs, cleaned them up and installed them into an entirely different working chassis (saving the parts from that one, of course), and returned it to my friend... he thought I had 'worked a miracle'. He had left the room for a few hours just as his Eico 70 was experiencing an output tube melt-down... Fortunately the panel breaker blew before the real-estate was threatened. To this day some 18 years later, he still believes that he has his original unit, only this time he pays attention to the bias and tube behavior. I don't charge people to indulge in my hobby, but I warned him that next time I would. I admire your perseverance, many would have returned the kluge to the customer and wished them the best of luck. And it does seem to be one helluvalot of money to spend for a badly conceived kit. Out of curiosity, do you think such kits are at all feasible in the real world? Do you think that: a) better instructions b) better parts-finishing c) better diagrams or some permutation/combination of the above could make such a kit workable for the average Jill or Joe? You mention that you had to design-build your own crossovers... They are not complicated, but do you think this should be "Factory" or at least the bits included? It seems to me from many thousands of miles away that the entire kit is an afterthought made from factory sweepings... But, thank you again for your painstaking description and tale. A significant example of "doing" over "blathering". Peter Wieck Wyncote, PA |
ER Audio ESL-3B speaker kit progress, 22 May07.
Patrick Turner wrote: Some of you may have been following my reported progress with trying to build a pair of ER Audio ESL-IIIB kits which were purchased by a customer of mine from http://www.eraudio.com.au/index.html I have had the job of "assembling" these kits to a satisfactory level of operation. I got started back in about February this year and could not proceed as quickly as planned because of difficulties encountered resulting from the poor design of the kits. Before people think I have no prowess at building kits or speakers or amplifiers, just take a look at my website at http://www.turneraudio.com.au and compare the amount of information and depth of understanding compared with the all too brief techno info at the ER Audio site. At the ER site there is no proper electronic schematic for the ESL3B as it should be, no impedance measurements, and no measured performance data. These should be stated with ESL, because some amps will NOT be able to drive the ER speakers, whereas the speakers at my site are all easily drivable, and everyone knows about SEAS drivers being OK, so nothing I have made is any worse than the best speakers made with SEAS drivers such as Sonus Faber and Vienna Acoustic. I gurantee a flat full range response, ER don't gurantee anything. I have now overcome most of the ERA problems; I was not warned by anything at the ER Audio site. Here is the history so far of what happened, and it includes process details and some solutions worth remembering. The kit was supplied with spacers already glued to the 1,200mm x 550mm frames for the 3 panel speaker. 8 of the 12 machine screws riveted to the 12 stator plates were too long, and I had to cut them down with a Dremel tool to 6mm. Failure to notice if the screws are too long will result in a completely stuffed panel, because the stators frames won't press down flat properly onto the frames they are glued into with polyurethane glue. The only real mistake I made was with the first attempt to stretch a membrane of the 3.5uM gossamer thin mylar membrane. It is just so delicate! It was easy to tear using tape and a spring balance for sequential tensioning. And sure enough it tore, and I had to begin again, and the second attempt went perfectly until I glued the first frame with its stators in place onto the surface of the stretched out membrane using super glue. Unfortunately, a pin hole of invisible size allowed super glue to seep through to the bench underneath, and the membrane was ruined as I lifted the panel off the bench. Its easy to sand it off the frame and clean up to do it again. Could practice make perfect? I was about to learn.... Use of superglue as recommended in the ERA 33 pages of kit instructions was abandoned!!! I sanded down the surface of the MDF sheet I was using as the bench top with very fine 600 grade wet and dry sandpaper to remove whatever might have caused a damn pinhole. The bench sits on top of a heavy oak dining table I built 31 years ago from thick oak planks. ( I don't have dinner parties anymore, and the accoutrements of a gentleman have more productive uses these days ) The third membrane went fine when I stretched it, and I used the polyurethane glue to glue to the frame after painting on the glue thinly to the plastic frame. I learnt that the easiest way to weigh down the frame on top of the membrane already stretched out on the perfectly flat solid bench is with about 24 house bricks. After lowering the frame with wet glue onto the membrane, cover the frame with a damp towel. The moisture in the towel will ensure the polyurethane glue cures well in 24 hours. Place the bricks on top of the towel gently without allowing the frame to slide around. When all bricks are placed, gently go to each prick and press down hard with about 20Kg in turn, and this will help remove air bubbles in the glue. The towel prevents brick particles falling into the speaker panel. You need to be very clean about everything with the construction; I used my loungeroom because of the good lights, and clean environment. Next day I very carefully cut around the edge of the membrane and I had a perfect looking membrane when I lifted the bricks and towel away and lifted the frame. The conductive strip of copper foil was placed on the second frame and there were no problems. This self adhesive strip 4.5m wide by about 0.2mm thick is actually the foil they use around bits of glass used in leadlighting windows, and is easily available. DON'T drill the 4.5mm dia holes for the 12 x 4mm dia plastic bolts too close to spacer edges or else the membrane will not glue to the spacer properly and will begin a tear at the hole. If you don't understand this, you will have torn membranes, and need to relocate bolt holes, after filling up wrong ones, and this is a PITA..... I applied the high resistance coating to the membrane. All seemed to go OK but I used twice more than recomended, and Rob Mackinlay from ER later said I shouldn't use too much. After waiting a week for the coating to cure, I completed the basic assembly with supplied plastic bolts and plastic surrounds and I had a basically completed speaker, but without the timber surround or box for electronics underneath. The kit does not include any surround timber frame or box, and one is left to make all that oneself, its rather like being given a speaker kit with drivers but without a box. I can only imagine the terrible attempts being made by amateur audiophiles who have no carpentry or joinery making skills or tools. You won't want to see their speakers pictured on the Web. Then came time to hook up the input transformer and build the not supplied board for a suitable cross over for the speakers. I designed and built the un-supplied crossover and required board. The electronic parts supplied were a regulated LV dc power supply which can be adjusted for its dc level. This then feeds a supplied EHT supply which converts the sub 10Vdc to up to about -5.5kV for application to the membrane. The EHT supply is connected with -EHT voltage taken to the copper foil strip around the frames and the ground terminal of the EHT supply is taken to the CT of the SUT secondary. The SUT is supplied, but has half the core size and half the primary turns really needed for saturation proof operation. I have advised ER Audio with full details of an alternative design for their transformer, and i look forward to them addopting my recomendations. The supplied SUT has far too thin P to S insulation, resulting in 390pF of shunt capacitance appearing across the secondary, which transforms to massive 3.16uF at the primary. The treble panel has 100pF capacitance which transforms to 0.81uF, and the total input capacitance seen by the amplifier = 4uF, ( about twice what Quad ESL57 managed ). The bass panel capacitance of 800pF transforms to 6.5uF at the primary, but the series resistance prevents this much C ever being experienced as a load on the amp, so bass panel C is quite entirely benign. I tried a very basic crossover network about which I will have more to say, and hooked up the speaker and tranny to an amplifier capable of 21Vrms max into a high Z load, and up to 70 watts into 3 ohms, 14.5Vrms. Output Z was 0.2 ohms, BW 7Hz to 30kHz, 2 ohms connected at low levels, and THD 0.2% at max po into 8 ohms, 50 watts, 18Vrms, and mainly class A with a quad of mosfets. I turned on the EHT and gradually increased the EHT until I heard all kinds of spluttery spittery sounds and saw numerous blue discharges occuring all over the panels. I backed off immediately until the noises stopped and conducted sound tests using pink noise and test gear as described in my speaker building pages at http://www.turneraudio.com.au/loudspeakers-diy.html Then I began testing the responses at 1M, 2M ,4M distances at a 1.2M off floor level, on axis, with the speaker taped temporarily to a stout dining chair I also built 31 years ago. Bottom of the speaker is 450mm above the floor, speaker is vertical. I got a truly appalling response. The sensitivity seemed appallingly low. For the same quite low level of pink noise, I needed maybe 5 times the voltage I'd need for my own Sublimes shown at http://www.turneraudio.com.au/loudspeakers-new.html The power handling was atrocious, and LF capablity suffered from arcing and distortions. My customer visted me in the middle of testing and was not impressed at all. We talked about quitting, but I ain't no bloody quitter. I obtained the loan of a high impedance HV probe to measure up to 20kV safely, and found that any EHT increase above 2.2kV cause horrid discharge noise and premature clipping. ESL sensitivity is about proportional to applied EHT voltage, and I wanted to be able to apply 5,000V if possible, like ESL57 and ESL63. I then thought that the arcing seen must be because the poor insulation qualities of the black powder coating on the suplied stators. So I stripped off membrane No 3, and coated all the stators with two generous coats of anti corona paint, Isonel 642, and put on a new membrane No 4 but with two very thin conductive coats on the membrane, this time using the right total amount and to get an even coating. I also placed in the pattern of 10 anti resonance silicone pads but that made no difference to following results. I re-tested after the rebuild and curing times, and although there was not such a lot of arcing and EHT leakage, the response and problems were quite unacceptable. I turned off the EHT supply, and considered using more membrane tension of 2Kg / 60mm of side length, not the low 0.8Kg recommended. ESL63 use 2.5Kg for the same material. Lots of crackling noises continued for minutes after turn off of the EHT and after the voltage had rapidly fallen to 0V. It was the membrane partially releasing from its stuck position. When I unbolted the two halves of the speaker the next day after the dismal tests, I found that about 70% of the area of both bass membranes had become glued to the stators on the side away from that where the membrane is coated. I was able to gently prise the membrane off the starors with a bit of bent copper wire poked through slots in the stators. Anti corona paint is slightly sticky with mylar. No wonder I had such horrible test results. But it had taken two attempts before I became aware of the problem and I guess that EVERY SILLY MAN WHO TRIES TO USE ABOVE ABOUT 3KV will have what I call membrane "stiction" problems. There are posts I've seen in these silly little private forums where they all bull**** to each other of guys cranking up the EHT and I believe they don't realize their problems. With stuck membranes, the speakers still work at mid & treble, but poorly, and definitely not as intended, and with queer bass. Back to my drawing board I went, and at this point I didn't think it would be wise to consult ER Audio for advice, and I posted on these groups to see if anyone else had had problems. One Collin Topps of the UK answered my initial posts to groups in private emails which began cordially, but ended rudely. Collin is the UK ERA sales rep. He said repeatedly nobody has had any problems building ER Audio panels. He refused to accept that I was having serious bothers, or offer any advice that was relevant and useful. Then he ended up telling me to sod off, and I thought that this technically dumb salesman in the UK acting for ER Audio as their sales agent has some basic things about public relations he has yet to learn. He'd sure never get a job selling anything I made. I continued to post on the panels and learn more about ESL construction from other ESL amateur productions around the world. Since then, I decided that the membrane must not be allowed to travel too close to a stator, ideally not more than half the actual distance between membrane and stator surface, so if this is 4mm, as it is in ESL57 bass panels, then 2mm is enough maximum movement distance. Quad achive this by using 2mm thick PVC plastic sheeting for bass stators, with conductive stator material being conductiove paint on the outside of the perforated plastic sheeting. So the membrane CANNOT move more than 2mm and cannot be less than 2mm away from the stator surface. The of force of electrostatic attraction increases proportionally to 1/d squared, so if d is only a few thousanths of an inch, F becomes huge. No wonder my ERA membranes were sticking like cling wrap around a pumpkin at the grocer. The bass panel membrane to stator distance in ERA panels is 2.4mm. I thought that if I applied about 0.8mm of non conductive material to the inside surface of the stator, It would keep the membrane getting too close to a stator, and the extra tension would always overcome the force caused by the EHT without signal. I'd have 1.6mm for membrane movement, not as much as in a Quad speaker, but enough. So I applied four coats of silicone paint made from roof and gutter silicone sealant bought for $5 per tube at a plumber's store. To coat all the stators for one speaker I used 1.3 tubes of silicone, and about 600ml of white spirit for thinning. The thinning is done by using a small cheap brush with dabbing action in a clean tuna fish can until the paint has thick honey consistency and no visible lumps. The silicone is applied by dabbing action with the brush laid flat on the perforated steel sheeting, not letting silicone close off perforation holes. It self levels fairly well, and partially wraps around the sharp metal edges of the holes in the stators, so probably enhances air flow caused by sound waves. 24 hours is fine between coats of silicone. It sticks well to the anti corona paint I already have on the stators. The silicone becomes rubbery, and smooth surfaced, even though some uneveness of this coating thickness occurs, but basically, I got the right amount of goop applied to all stator surfaces. I finally stretched membrane No 5 last week and have re-assembled the speaker for a new test. After the frame was first glued to the stretched and much tighter membrane, I still found the membrane tended to stick to the stator if pressed over to it gently by hand. So I then bought a small can of Johnson's Baby Powder and squirted in a lot of powder through perforations, and with an air blower, blew it all around everywhere. Then i sucked off the excess woth a gentle vacuum cleaner. On the opposite second frame and stators, i just dusted the powder on and removed excess with vacuum. The panel was then re-assembled. Did my ingenuity prevent the problems I was having? After connection of the speaker to the amp and without signal, I raised the EHT and at 3.2kV while I watched the bass membranes carefully I saw them whip over to a stator and remain hard against it. Hmm, same old problem. However, when i reduced EHT, the membrane let go without all the crackling sounds they'd made previously after turn off of the EHT supply. The powdered layer of rubber was doing the right kind of trick in preventing stiction. I was able to leave the EHT on all night at 3kV, but just occasionally, some small click noise would occur, so i have settled on having 2.7kV as the maximum EHT voltage which could be safely applied to these panels before problems would occur. I began to seriously test the speaker response and do serious comparisons again with my own blameless Sublimes. They sit side by side, and comparisons can be fairly made, same room, 200Cubic metres, well out from a wall, well damped etc. The same amps, test signal, test gear and mic is used to eliminate any chance of making an unfair comparison. Finally, I got the speakers to measure +/- 2dB between LF pole = 35Hz and HF pole = 22kHz, and to give as flat a response as I could get without adding a ridiculous number of crossover compensation networks. This response was measured at 3M with mic 800mm above the floor, and about exactly how they will be listened to in my customer's room, which is not quite as good as my own, but measurement of his existing speaker response has been little different to what i get in my rooms. If I get speakers to sound well here, they always travel well. My impressions with the sound with music is good, but the 50 watt class A amps I have been using for trials run completely out of headroom at only modest levels equal to about 1/3 watt average into my Sublimes which are 5.6 ohms average, and have 88dB/W/M watt sensitivity. After numerous calculations, I figured I needed 5 times the applied voltage for the same SPL with ERA panels compared to my own speakers. At least a 100 watt amp would be needed for quite modest levels of sound, not because 100 watts would ever be generated, but merely to get enough voltage. Collin Tops said he was using an SET amp with 16 watts only, and maybe he likes quietspeakers. But I prefer loudspeakers. And for these ERA quietspeakers, there is not the slightest bit of speaker protection circuitry included as it is in Quad ESL63. What is the safe maximum voltage? not as much as for Quads, that's for sure. Anyway, I did clip the 50 watt amp a few times when i tried to go loud with some busy Salsa music from Buena Vista Social Club, and nothing bad happened, so the 6 coats of goop I have on the stators seemes to resist arcing. A 16 watt SET amp with Rout 2ohms would be a horrible thing to drive such ESL. There would be a serious HF roll off, but perhaps Collin is an old giza with stuffed hearing, and so may not mind if the HF pole = 6kHz. And without my networks and crossovers, the response could be worse, peaked up high between 500 and 6kHz, ie, without bass or treble. He will have to conduct all the same well conducted tests i have done before he'd ever know WTF he's actually built. He should not be offended when I say I don't trust what salesmen tell me. Nobody from ERA has had the courage to discuss their speakers in the public forums. I have just measured the Z, and with the details of networks below got the following Z figures:- 10Hz, approx 80ohms, 20Hz, 41, 50Hz, 14, 60Hz, 11, 80Hz, 10, 110Hz, 11, 200Hz, 18, 300Hz, 20, 500Hz, 19, 1kHz, 15, 2kHz, 11.5, 10kHz, 5, 20kHz, 3, 40kHz, 2. If you plot the above points on a graphed sheet of log paper, and join the dots with gentle curves and you will have the Z. The average Z between 50Hz and 2kHz = 14 ohms. Therefore a tube amp set up for a match to 16 ohms will work, but it'd need to be able to make 30Vrms, which is 64 watts into 14 ohms. The amount of signal above 2kHz which feeds the low Z average of 5ohms between 2khz and 20kHz is small, and as long as the Rout 0.5 ohms there will not be a serious loss of HF detail. One of my 8585 tube amplifiers with a quad of KT90 in PP per channel is powering 3 stacked pairs of ESL57 no problems, even though the Z = 0.6 ohms at 18kHz. But 16 watts from SET would be hopless, unless you had the speakers so close they are like giant ESL headphones. DO NOT use the recommended circuit resistances so vaguely shown in the ER instructions. I found that the best way to hook up the ESL-3B speakers is as follows:- BEFORE the the input to the primary of the step up transformer, ( SUT ):- Make a series L + R network of 4mH plus 27 ohms. Connect this across the P winding. Connect one end of the P winding to the 0V terminal for the black lead from the amplifier. To the other live primary end, connect a series C & R network of 150uF plus 1.5ohms across to the speaker terminal to which the red wire from the amp connects. These two input networks will have several effects. The 27 ohms plus 4mH makes the input loaded with 27 ohms at low F, thus damping the low Z of the series 150uF and primary shunt inductance of 32 mH. The 150uF will prevent LF entering the speaker and causing the rather poor quality SUT from saturating all too easily with high transient LF voltages. The -3dB cut off is at 50Hz, and the attenuation is second order, barely enough. To get better headroom for these speakers, use a second input cap in series of 100uF, giving -3db at about 100Hz, then use a sub. More signal will be then applicable above 100Hz. The 1.5 ohms adds to the 0.5 ohms of SUT winding resistance which is important to damp the series resonance between the awfully high amount of shunt capacitance in the SUT and the leakage inductance at around 20kHz. Therefore input resistance is a minimum of 2ohms by 50kHz, so not many amps should blow up. AFTER the secondary of the SUT, place the following networks from each end of sec to the bass panel terminals:- You will need the following parts, 16 x 100k resistors, metal film, 1%, 2 watt rated. 2 x 0.0033uF capacitors rated at 4kV. Find good quality polypropylene caps. To each bass stator, connect 100k to a pair of common points for the rear and front pairs of bass panels, Then series 4 x 100k to make 400k from each common point to the ends of the SUT secondary. To each treble stator, connect a parallel pair of 100k to make 50k to a pair of common points for front and rear stators. From the common points, connect the 0.0033uF to the sec ends of the SUT. The 0.0033uF plus 50k form a CR HPF. MAKE SURE the treble panel with its crossover is REVERSE PHASE CONNECTED TO THE BASS PANELS. The -3dB points in the signals in the electronic circuit thus created is 160Hz for bass, with signal rolling off at 6dB/octave above 160Hz, and 700Hz for the treble panels, also rolling off at 6dB/octave. Keeping pass signals out of the treble panel is a good idea. The speaker phase shift will be maximally quite large, but maybe under 60degrees, but I found the treble acoustic signal produced by the bass panels will affect the treble panel badly if not phase reversed ( like many other dynamic speakers ), and despite the attenuation by the R & C filter LPF effect of bass series R and the bass panel capacitance which totals 800pF. The ONLY way I could flatten the response and remove what was a wide 6dB dip in the resonse at 5kHz with reverse phase connections. This what I measured, and the acoustic response has little corelation to the signal applied. I will perhaps draw all the relevant curves of bass and treble signals applied and and include all this info at a website page. I hope to include a schematic of the equivalant LCR model of the the panels and SUT. I hope there would be a net positive result amoung builders of ESL. This should all have a very positive effect on understanding of what is really involved to make a pair of ESL speakers. Hopefully, all of what i say will fertilize the minds who created the ER Audio ESL speakers. They can scream long and hard at my critique, and i don't give a ****, their marketing is quite deceptive, and they say it'll be easy, and take only so long, but no, its not true, and they are bull****ting, and the total time I will end up spending on R&D, and patching up the mess of the thing they supplied plus do all the woodwork will amount to 10 times the time they say. My customer here was lulled into the project, along with me, under what now seem like false statements about the product. Had I known of all the difficulties and parts quality and non inclusions, i would never ever have agreed to my building of one of these kits after my customer bought it. He isn't technically minded, and could NEVER EVER have successfully built a kit from ERA. If I allowed quite low trade rates of $50 per hour to build these speakers and fix problems and do R&D, I would find I would be entitled to claim a payment of maybe $5,000 for the labour of building these speakers, plus the cost of supply of items not included, about $400. being a gentleman I won't ask more than a fraction of the figure from my customer, but frankly, the sooner I see these speakers leaving my workshop, the better, and I don't ever want to build another pair that I did not fully design myself!!!!! The original kit price was $2,000, and so the whole deal of up $7,400 value is quite poor value when a fully restored/rebuilt pair of Quad ESL57 could be had for about $4,000 from one John Hall in Melbourne. I have a Quad ESL57 which is unrestored and it even outperforms the ERA on most counts. How anyone could say the ERA speaker is better product than a Quad ESL57 or ESL63, as some have suggested is quite beyond me; maybe these people had old speakers with lots of faults, and replaced them with ERA because they thought they'd be better. The other complaint I have about the ESL3B is that its ONE panel, not two bass with one treble, like ESL2B. This means that if a membrane tears or ****s up in just one of the 3 sub panels, the WHOLE 3 subpanels have to be fixed, rather than just fix one of the 3 sub panels. There is BS spiel about why the ESL3B is a better than others, but ERA are pushing the flat ESL3B because it appears to me the cost of production is less for the less complex product. but the repair bills for YOU, the buyer, will always be higher. All the comparisons one reads make silly one liner statements without the pages of detailed back ups. So don't make me waste more time reading your replies which are not backed up with facts. Patrick Turner. I admire your perseverance, Patrick, I really do. But by now you've put in so much labor, a pair of Quad electrostats will be cheaper. Thanks to The Boss I didn't go down your route. I enjoyed making various quarter wave tapered pipes that Andre designed, and his Impresario which my wife banished to the basement of our summer house because it is so big, and horns for which Andre got me factory wood and held my hand by e-mail through the assembly and modification and veneering. Then I thought I was ready for electrostats. The Boss said he would design me a direct drive tube amp if I actually managed to build something first that worked with a stepup transformer from Sowter. But I found a Dutch site and got some Google translations, and Andre made me a couple more translations, and they frightened me right off. Like The Boss said all along, it is much cheaper to buy Quads than to mess around with DIY panels. They never work right. I still dream of making my own electrostatic headphones though for the time being, again on Andre's recommendation, I've just bought a pair of Stax and built one of Andre's octal OTL amps to drive it. On the scale of electrostatic earphones, a reasonable DIY result ought to be possible. Maybe not economical considering how cheap Stax earhpones are but possible, don't you think? Kind regards, Gray Glasser |
ER Audio ESL-3B speaker kit progress, 22 May07.
snip my own stuff and a couple of inane comments by others, Professor, What you described was a horror story for a layman. With all said and done, how do the bloody contraptions sound? The sound is "interesting", goodish, and I will see what my customer thinks when we sit down to a couple of CDs next Saturday using his 120W Musical Fidelity A3 amplifier. But they are not loudspeakers, just quietspeakers. An amp designed for 50 watts into 5 ohms doesn't have enough voltage headroom produce enough level. The limiting factor is bass levels. if the bass panels had twice the area, much less membrane excursion woulod be needed, and this would allow the FRED effect, full range electrostatic driver. I think perhaps if I abandoned the need for deep bass production below 100Hz on these units, I could safely apply twice the signal, and get a lot more volume. But then my customer needs the extra bass speakers. If anyone buys the kits as is, I'd recommend they take the stators to a guy who can cut out shapes in sheet plastic, and have them create perforated 0.8mm thick plastic PVC sheet to the same pattern of the steel stator holes. This could then be glued well on the inside of the stators to "hold off" the membrane from trying to stick to the stators. But I wouldn't stop there. I'd use a larger stator to membrane distance, same as Quad ESL57, and use similar materials. Trouble is by the time I describe all the things one SHOULD do to make the kits world leading kits, one wouldn't bother to buy the kits at all, unless ER Audio incorporate what I am saying. I suspect they won't, perhaps because of the stocks they want to sell. They won't alter everything just because some self taught audio lunatic in Canberra wants to tell them how they ought to design their product. What I am suggesting is rarely ever welcomed as something to fertilize minds to make something better grow. Starting about NOW. The Quad ESL57 treble arrangement has 1/2 the distances of the bass panels, and much lower EHT and 1/2 the signal drive levels, so the mid/treble panel is smaller, lower C, and really, methinks its a better design for treble. However, the clearance distances and EHT could be higher, like in Quad ESL63, but then the signal drive must be higher. There are 5 things that are basically balanceable against each other, area of the panels, bandpass of the panels, distances between stators and membrane, signal voltage drive, EHT levels. Coating of the membrane is critical, but easy to do once youv'e done a couple. The design of the step up tranny is critical, and the higher the voltage ratio, the higher the Z ratio, and Quad's ESL57 potted and waxed SUT is a lesson to us all about how to do things right. In ESL63, Quad made things easier for themselves by using TWO trannies, one for each phase applied to stators. Its vitally important to keep insulation thickness between interleaved windings as thick as possible to curtail shunt capacitance which appears at the input as Z ratio x Cshunt at the sec. Braun made ESL57 variety in a panel size that was 1.5 times as high as the old '57. This is 1/2 way to having a stacked pair of 57. ppl who have stacked ESL57 seldom complain about bass being missing, so why not just have a similar design to '57 that is about 1.5M high, same width. The work involved isn't much more than with a single panel equal in area to '57. Capacitance rises though when the area increases, and thus its harder for some amps to drive them. But careful SUT design avoids the worst of the C. The only panel needing to be directly connected to the SUT sec is the small treble panels. The real enthusiast would never buy any kit, he'd draw up his design and make his calculations, after learning enough, and just do it. Apart from the SUT, the expenses for materials for two large sized panels can easily be less than $300. Getting anyone to wind the SUT with perhaps 10,000 turns of 0.2mm dia wire for the secondaries is a bother, so the enthusiast will make a lathe and wind his own. This is what I have done about OPTs. Using a large core of about 5Kg with large window area permits less turns, so less self capacitance of windings, and less leakage L and thicker P-S insulation. The SUT for ESL is very much like an OPT, except that its step up, not down, and that the V ratio is much higher, so the capacitance must be very low. The material costs in a 6Kg tranny are about $15 per Kg max, or $90. The rest is labour, so for the enthusiast who refuses to go to pubs, watch TV, dither about on the PC all day and night, he will find the time as was done in the past to do it all himself. We have become a lazy plug and play society. When I was 29, I built all my own furniture, a double garage which is a fine workshop now, all in my spare time after work in a regular day job. I also found time to build a decent pair of speakers, I was BURSTING with energy i could only be proud of, and all the idiots at the pub and stupid TV shows at night meant nothing to me. I doubled the size of the house I bought in the next few years after that. My energy and clear minded approach probably saved me an enormous sum of money paid to others. Patrick Turner. west |
ER Audio ESL-3B speaker kit progress, 22 May07.
Peter Wieck wrote: You have my deepest sympathies. This reminds me of some of the items that have crossed my bench for repair where the owner has a sentimental reason or some such that makes even the most irrational approach feasible. One such case, I actually took the few useable parts out of the item (one output transformer, a choke, front panel and knobs, cleaned them up and installed them into an entirely different working chassis (saving the parts from that one, of course), and returned it to my friend... he thought I had 'worked a miracle'. He had left the room for a few hours just as his Eico 70 was experiencing an output tube melt-down... Fortunately the panel breaker blew before the real-estate was threatened. I am re-engineering a stereo Woodham CR amp made in the UK. This nice looking amp has reliably produced clouds of smoke. It will be totally re-built, using my own circuitry. It was theraputic to remove all the terribly complex pcb to the rubbish pile, and saw a big hole in the case bottom to allow service access, and fix in a proper top chassis plate. To this day some 18 years later, he still believes that he has his original unit, only this time he pays attention to the bias and tube behavior. I don't charge people to indulge in my hobby, but I warned him that next time I would. I have to charge, its my living. I admire your perseverance, many would have returned the kluge to the customer and wished them the best of luck. And it does seem to be one helluvalot of money to spend for a badly conceived kit. Out of curiosity, do you think such kits are at all feasible in the real world? Do you think that: a) better instructions b) better parts-finishing c) better diagrams If all 3 things are improved, yes, the ESL kits could be equal to a Martin Logan, Quad, et all, and still less than 1/2 the prices for the high end names. Anyone building an ESL kit should salute the High End names for charging so much, because that high price gives them a chance to compete. or some permutation/combination of the above could make such a kit workable for the average Jill or Joe? Frankly, ppl used to putting a dynamic speaker kit together with nothing more than a screw driver and bottle of wood glue are in for a real shock woth an ESL kit. Its MUCH harder to get right. You mention that you had to design-build your own crossovers... They are not complicated, but do you think this should be "Factory" or at least the bits included? The "Factory" has not really done any R&D, other than guessing their way to good sound. I've done more in a couple of months than they seem to have done. I finally evolved the crossover R values by trial and measurement after intial calcs. It was a surprise to find that the signal applied to the bass panels has its F2 pole at 160Hz and rolls off at 6dB/octave, and and yet the acoustic response was essentially flat from 35Hz to 2kHz. So the bass panels have increasing sensitivity at 6dB/octave if fed with a flat signal, so you mustn't do this, because if you did the response would be an arch, like the Sydney Harbour Bridge, and the sound would be badly unbalanced with neither bass or upper treble. I measure things. I have serious technical expectations. I expect ruggedness, and simplicity, and ability to provide louder sound than I ever might use, ie, real headroom, sensitivity, and absense of arcing and BS stiction effects. Even after taking steps to limit the membrane travel, i was able to turn up the EHT and just watch the membrane move over to be hard against a stator. I'd back off the EHT, and it't re-centre, and I could repeat it. From this I can only think that ALL their bass panels would behave similarly. So the amount of EHT is limited to around -2,700V, thus limiting sensitivity. If the step up tranny ratio was increased from the existing 1:90 ratio, then the impedances all reduce; a rise of turn ratio to 1:127 would halve the impedance. There is a whole array of things need addressing and balancing. Peter Walker spent many years developing his line of ESL. It seems to me from many thousands of miles away that the entire kit is an afterthought made from factory sweepings... I wouldn't say the short comings are totally bad. I'd rather think positive, and hope the kit makers step up the quality. There IS a market for ESL, somewhat limited by the huge prices of new ESL speakers. There is about enough collective experience from the pioneers like Peter Walker and his mate Peter Baxandal to allow any keen person to develop decent ESL panels. Its all been done before. Patrick Turner. But, thank you again for your painstaking description and tale. A significant example of "doing" over "blathering". Peter Wieck Wyncote, PA |
ER Audio ESL-3B speaker kit progress, 22 May07.
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ER Audio ESL-3B speaker kit progress, 22 May07.
"Patrick Turner" wrote in message ... Some of you may have been following my reported progress with trying to build a pair of ER Audio ESL-IIIB kits which were purchased by a customer of mine from http://www.eraudio.com.au/index.html SNIP Urk. doesn't sound like fun to me. BTW: If you need a proper electrostatic Voltmeter, let me know. I have an ancient, but very good one. It's big and delicate. I wouldn't freight it to you, but would deliver personally. Or you can collect. I found it useful when servicing some Accoustats awhile back. They use a 500M Ohm series resitor in the HT section. -- Trevor Wilson www.rageaudio.com.au -- Posted via a free Usenet account from http://www.teranews.com |
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